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Well ID: 37-063-36263 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Indiana | |
Municipality: Canoe Township | |
Operator Name: ALLIANCE PETRO CO LLC | |
Well Pad ID: | |
Farm/Lease Name: MAE BELLE STATES 2 | |
License Status: | |
Spud Date: | |
Permit Date: 2008-10-10 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.851536 | |
Longitude: -78.982911 |
Date | Event |
---|---|
2008-10-10 | New Permit Application |
2009-03-24 | Performed Spud Operation |
2009-03-26 | Drilling Completion |
2010-08-03 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2008 | CONSOL GAS CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2009 | CONSOL GAS CO | 14929.75 | 365 | 0.00 | 0 | 0.00 | 0 |
2010 | CONSOL GAS CO | 10,607.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | CONSOL GAS CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | CNX GAS CO LLC | 8,696.00 | 366 | 0.00 | 0 | 0.00 | 0 |
2013 | CNX GAS CO LLC | 7,292.30 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | CNX GAS CO LLC | 6,744.50 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | CNX GAS CO LLC | 5,008.03 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | CNX GAS CO LLC | 3,800.48 | 366 | 0.00 | 0 | 0.00 | 0 |
2017 | CNX GAS CO LLC | 4,856.48 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | CNX GAS CO LLC | 2,400.93 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2009 | CONSOL GAS CO | Fracking Fluid | 300.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0091472 |
2009 | CONSOL GAS CO | Brine | 328.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0091472 |
2009 | CONSOL GAS CO | Brine | 74.00 Bbl | Injection Disposal Well | PA101656 |
2009 | CONSOL GAS CO | Fracking Fluid | 1,400.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0095443 |
2010 | CONSOL GAS CO | Produced Fluid | 80.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0020346 |
2010 | CONSOL GAS CO | Produced Fluid | 13.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0091472 |
2011 | CNX GAS CO LLC | Produced Fluid | 75.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095273 |
2012 | CNX GAS CO LLC | Produced Fluid | 123.00 Bbl | Injection Disposal Well | 34-007-22038 |
2013 | CNX GAS CO LLC | Produced Fluid | 34.49 Bbl | Injection Disposal Well | 34-013-20609 |
2013 | CNX GAS CO LLC | Produced Fluid | 63.00 Bbl | Injection Disposal Well | 34-119-28776 |
2014 | CNX GAS CO LLC | Produced Fluid | 20.00 Bbl | Injection Disposal Well | 34-155-21894 |
2014 | CNX GAS CO LLC | Produced Fluid | 20.00 Bbl | Injection Disposal Well | 34-155-21893 |
2014 | CNX GAS CO LLC | Produced Fluid | 20.00 Bbl | Injection Disposal Well | 34-155-23203 |
2016 | CNX GAS CO LLC | Produced Fluid | 65.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
2016 | CNX GAS CO LLC | Produced Fluid | 65 Bbl | CENT WASTE TRT FAC NPDES | PA0095273 |
2016 | CNX GAS CO LLC | Soil Contaminated by Oil | 13.64 Tons | LANDFILL | CID # 28726 |
2016 | CNX GAS CO LLC | Soil Contaminated by Oil & Gas Related Spills | 13.64 Tons | LANDFILL | CID # 28726 |
2019 | ALLIANCE PETRO CO LLC | Produced Fluid | 69.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1780695 | Primary Facility | 2009-03-27 | Drilling/Alteration | No Violations Noted | drilling complete - not equipped/pit ok/E&S ok |
2286331 | Primary Facility | 2014-07-09 | Routine/Complete Inspection | No Violations Noted | |
2449485 | Primary Facility | 2016-02-15 | Administrative/File Review | In Compliance with Policy | SPILL.
ON 2/15/16 AT 1248, A SPILL WAS REPORTED TO FIRST CHOICE TAS BY OPERATOR REPRESENTATIVE RICHY VROBEL. SPILL REPORTED TO BE CONTAINED. NO WATERWAYS REPORTED TO BE AFFECTED. OPERATOR REPORTS RELEASE RESULTED WHEN VALVE CAME OFF WHILE COLLECTING A SAMPLE. |
2449503 | Primary Facility | 2016-02-16 | Administrative/File Review | In Compliance with Policy | Admin inspt in response to inspection ID 2449485 for 2/15 reportable release of brine water.Upon receipt of spill notification, Dept contacted Opr rep R.Vrobel via phone at 1007.According to Mr. V, the release resulted when plug was being removed from brine tank and whole valve came off of nipple, releasing 15 bbl of brine into earthen dike.Release stopped by screwing valve back onto nipple.Mr. V stated that brine water did not leave earthen dike and no waterways have been impacted.A water truck was immediately dispatched to site to empty remaining fluids from tank and to remove standing fluids from earthen dike. Mr. Vrobel believes that fluids did not saturate ground as it was frozen at time of release.The amount released was determined by measuring level of brine water in tank before and after release.Per Mr. V,removal of all contaminated materials is scheduled for tomorrow (2/17) at 0900.Spill occurred on 2/15 at 1230 and was subsequently reported to First Choice TAS at 1248.A FUI will be conducted. |
2450320 | Primary Facility | 2016-02-16 | Incident- Response to Accident or Event | Violation(s) Noted | Inspection in response to Operator report of a 15 bbl release of brine into earthen dike (Inspection Record #2449485).
At time of inspection brine tank located in earthen dike. Valve at bottom of tank appears attached. No liner in dike observed; some fluids present in dike. It appears excavation of contaminated soils has not yet begun because of inclement weather. Operator anticipates beginning excavation on 2-17-16. Department recommends Operator install temporary BMP's prior to beginning earth moving activities to prevent a subsequent potential pollution event. Site and access road snow covered. Violation being issued for discharge of brine or other fluids on or into the ground. |
2463375 | Primary Facility | 2016-03-10 | Compliance Evaluation | In Compliance with Policy | Admin CEI inspection to Inspection Record #2450320 where violation issued for Operator reported discharge of brine.
Department received 15 day response to NOV from Operator on 2-29-16. Operator is In Compliance with Policy at this time in as far as Operator intends to follow the Alternative Remediation requirements for clean-up of release and intends to test for the following compounds/Anions: aluminum, Barium, Boron, Iron, Lithium, Manganese, Selenium, Strontium, Vanadium, Zinc, and Chloride. A follow up inspection will be conducted to ensure site has been permanently stabilzed. Additional violations may be forthcoming pending follow up inspection. |
2475448 | Primary Facility | 2016-04-04 | Administrative/File Review | In Compliance with Policy | Admin inspection to Inspection Record #2450320.
Department has received Site Characterization Report for this site. Operator is utilizing Alternative Remediation to remediate a 15 bbl release of brine. Department contacted Operator Rep Jessie Valentine by phone on 4-4-16 to request resubmittal of Site Characterization Report because of error that lists property owner as CONSOL Energy. UPDATE: 4-11-16: Operator contacted Department and stated a corrected SCR will be mailed. |
2475474 | Primary Facility | 2016-04-18 | Administrative/File Review | In Compliance with Policy | Admin inspection to Inspection Record #2450320.
Operator Rep Jessie Valentine contacted Department by e-mail on 4-11-16 and stated that the correction to the Site Characterization Report has been made and the corrected report will be mailed that same day. UPDATE: 4-18-16: Department received corrected Site Characterization Report. |
2486672 | Primary Facility | 2016-05-11 | Routine/Complete Inspection | No Violations Noted | At time of inspection no E&S issues observed on access road or on site.
Well appears to be in production. Well label present and legible. Brine tank located in earthen dike appears structurally sound. |
2501754 | Primary Facility | 2016-07-06 | Routine/Complete Inspection | In Compliance with Policy | At time of inspection well appears equipped for production. No E&S issues observed in relation to the access road or well site. Well tag present. Brine tank located in vegetated dike appears structurally sound.
On 2-15-16 a release of 15 bbl of brine was reported to the Department. Operator stated in the 15 day response that on 2-17-16 Spartan Specialty was to excavate approximately 13.65 tons of soil from the dike. At the time of this inspection it does not appear that the excavated area is seeded or mulched. Inspected with J. Gorman. UPDATE 7-11-16: Department contacted Operator Rep Jessie Valentine by phone to verify excavation was completed and area was seeded and mulched. Mr. Valentine stated he would visit the site on 7-14-16 and follow up with Department. Photos from the 7-6-16 inspection are attached to this inspection report. |
2504257 | Primary Facility | 2016-07-15 | Administrative/File Review | In Compliance with Policy | Admin inspection to inspection record #2501754.
Operator Rep Jessie Valentine e-mailed Department after his site visit on 7-14-16. Mr. Valentine stated that the excavation by Spartan Specialty was done under and around the brine tank, not throughout the whole dike area. Mr. Valentine tested random spots throughout the dike area with a conductivity meter and all sampled locations showed low conductivity readings. Mr. Valentine also stated the area in the dike is "very rocky and hard" therefore the newly planted vegetation may not have grown. It appears that Operator is in compliance with policy at this time. |
2550408 | Primary Facility | 2017-01-04 | Routine/Complete Inspection | No Violations Noted | On-site inspection conducted to monitor site remediation as a reportable release of production fluids previously occurred at this site. Violations were issued for this reportable release under inspection record 2450320 (enf ID 334645) and subsequently corrected under inspection record 2463375.
At time of inspection, site is permanently stabilized with >70% uniform and adequate vegetative growth, appears restored. Access road stabilized. Well label present on brine tank. Department recommends Operator install well tag on well in a legible, visible, and permanent manner per current regulations. According to records, drilling occurred 3/24/2009-3/26/2009. Brine tank located on plywood base within a vegetative dike. Brine tank appears sound. Area within dike where release was previously reported to have occurred (inspection IDs 2449485, 2449503) appears stabilized with rock and vegetation. In accordance with the Spill Policy, the 15 day initial written report was received on 2/26/2016 notifying the Departme |
2769345 | Primary Facility | 2018-08-30 | Routine/Complete Inspection | No Violations Noted | Well appears to be in good working condition. |
2847707 | Primary Facility | 2019-03-04 | Administrative/File Review | No Violations Noted | Start Sheet created for file. |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2450320 | 746083 | 2016-02-16 | 2016-03-10 | 78.57(a) | Environmental Health & Safety | Operator written response states they will follow Alternative Remediation for spill clean up. |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
746083 | 334645 | NOV - Notice of Violation | 2018-03-12 | ||||
746083 | 362231 | CACP - Consent Assessment of Civil Penalty | 2018-03-12 | $4,500.00 | $4,500.00 |
For data sources see[7]