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37-063-36808

Well Details

Well ID: 37-063-36808
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Country: United States
State: Pennsylvania
County: Indiana
Municipality: Young Township
Operator Name: ALLIANCE PETRO CO LLC
Well Pad ID:
Farm/Lease Name: CURTIS F POOLE 5
License Status:
Spud Date: 2010-07-21
Permit Date: 2010-04-15
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.580972
Longitude: -79.345694

For data sources see[1][2][3]

Well History

Date Event
2010-04-15 New Permit Application
2010-07-22 Performed Spud Operation
2010-07-27 Drilling Completion
2010-07-30 Perforation
2011-01-19 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2010 PHILLIPS EXPLORATION INC 3,604.00 110 0.00 0 0.00 0
2011 PHILLIPS EXPLORATION INC 10,616.00 351 0.00 0 0.00 0
2012 XTO ENERGY INC 7,975.00 366 0.00 0 0.00 0
2013 XTO ENERGY INC 5,721.00 364 0.00 0 0.00 0
2014 XTO ENERGY INC 4,322.00 252 0.00 0 0.00 0
2015 XTO ENERGY INC 4,034.49 364 0.00 0 0.00 0
2016 XTO ENERGY INC 2,903.10 365 0.00 0 0.00 0
2017 ALLIANCE PETRO CO LLC 2,400.00 334 0.00 0 0.00 0
2018 ALLIANCE PETRO CO LLC 3,081.00 365 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2010 PHILLIPS EXPLORATION INC Fracing Fluid Waste 17.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095273
2010 PHILLIPS EXPLORATION INC Fracing Fluid Waste 1.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0020346
2010 PHILLIPS EXPLORATION INC Fracing Fluid Waste 13.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095443
2010 PHILLIPS EXPLORATION INC Fracing Fluid Waste 5.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0091472
2010 PHILLIPS EXPLORATION INC Fracing Fluid Waste 15.00 Bbl PUBLIC SEWAGE TREATMENT PLANT PA0026310
2010 PHILLIPS EXPLORATION INC Fracing Fluid Waste 1.00 Bbl PUBLIC SEWAGE TREATMENT PLANT PA0026034
2010 PHILLIPS EXPLORATION INC Fracing Fluid Waste 110.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE 301353
2011 PHILLIPS EXPLORATION INC Produced Fluid 10.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095443
2011 PHILLIPS EXPLORATION INC Produced Fluid 10.00 Bbl PUBLIC SEWAGE TREATMENT PLANT PA0026310
2011 PHILLIPS EXPLORATION INC Produced Fluid 10.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095273
2011 PHILLIPS EXPLORATION INC Produced Fluid 10.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE 301353
2012 XTO ENERGY INC Produced Fluid 39.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095273

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1874857 Primary Facility 2010-03-26 Routine/Complete Inspection No Violations Noted Well staked. Site not constructed.
1901132 Primary Facility 2010-07-28 Drilling/Alteration No Violations Noted
1904398 Primary Facility 2010-07-27 Routine/Complete Inspection No Violations Noted Site id sign in place. E&S plan on site. Waiver from distance restriction to Blacklegs creek and associated pond approved on 3/26/10.
1904400 Primary Facility 2010-07-29 Routine/Complete Inspection No Violations Noted Site id sign in place. E&S plan on site. Waiver from distance restriction to Blacklegs creek and associated pond approved on 3/26/10.
1904405 Primary Facility 2010-08-04 Routine/Complete Inspection No Violations Noted Site id sign in place. E&S plan on site. Well just recently drilled, not equipped for production.
1907856 Primary Facility 2010-08-17 Routine/Complete Inspection No Violations Noted
1966290 Primary Facility 2011-04-14 Site Restoration No Violations Noted Well tag in place. Well is equipped for production. Drilling completed 7/27/10.
2252002 Primary Facility 2014-03-10 Administrative/File Review In Compliance with Policy SPILL -Notification of release of approximately 1 barrel of a crude oil/produced water mixture at approximately 12:15pm on 3/10/2014 (call received approximately 2:01pm on 3/10/2014). Operator informed me that two roll offs on the way to the site; excavator, dump truck, vac truck, and water truck on site. Oil absorbants etc. are down.
2253204 Primary Facility 2014-03-11 Incident- Response to Accident or Event Violation(s) Noted On-site inspt in response to admin inspt 2252002 for reportable release of approx 1 bbl mixture of crude oil/production water.Well-tender Gordon Bish on-site.According to Mr. Bish, wellhead split, spraying oil, brine water, "white water" out of crack.Occurred b/w 3/6/14 to morning of 3/10/14.Lease opr discovered on 3/10/14 at 1200.Production equipment disconnected from well.Currently excavating impacted soils, all visible oil removed.Preparing to re-locate brine tank to excavate soils underneath.Two roll-off boxes on-site, addit'l boxes to be brought on-site.As pond is located approx 125 ft down-gradient from site of release, Dept recommends sampling is conducted to ensure contaminants did not reach waters of the Commonwealth.Opr to follow Act 2 guidelines for site remediation.Drilling occurred 7/21/2010-7/27/2010.Well label present.Dept recommends Opr monitor/maintain access road as increased traffic due to clean-up efforts could potentially result in an accel E&S pollution event.Viols issued under 25 PA CODE 78.54, 78.57A & 58 PA CODE SWMA 301
2253688 Primary Facility 2014-03-13 Follow-up Inspection Outstanding Violations - No Viols Req'd On-site inspt in response to violations issued under inspt record 2253204 (enf ID 308677) for reportable release of approximately 1 bbl mixture of crude oil/production water.
2293627 Primary Facility 2014-07-31 Follow-up Inspection Outstanding Violations - No Viols Req'd On-site inspt in response to violations issued under inspt record 2253204 (enf ID 308677)
2321455 Primary Facility 2014-11-12 Follow-up Inspection Outstanding Violations - No Viols Req'd FUI in response to violations issued under inspt record 2253204 (enf ID 308677) for the 3/10 reportable release of crude oil/production water.
2346572 Primary Facility 2015-02-25 Compliance Evaluation No Violations Noted Admin CEI in response to violations issued under inspt record 2253204 (enf ID 308677) for the 3/10 reportable release of crude oil/production water.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2253204 690914 03/11/2014 2014-03-11 78.54* - Failure to properly control or dispose of industrial or residual waste to prevent pollution of the waters of the Commonwealth. Environmental Health & Safety

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
690914 308677 NOV - Notice of Violation Comply/Closed 2015-10-13

For data sources see[7]

References