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Well ID: 37-065-20004 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Jefferson | |
Municipality: Porter Township | |
Operator Name: EQT PROD CO | |
Well Pad ID: | |
Farm/Lease Name: JW SNYDER 2 | |
License Status: Plugged and Abandoned | |
Spud Date: 1956-05-19 | |
Permit Date: 1956-04-05 | |
Well Type: UNDETERMINED | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.943283 | |
Longitude: -79.195218 |
Date | Event |
---|---|
1956-08-02 | Drilling Completion |
1956-12-30 | Newly Drilled |
2018-06-04 | Begin Plugging |
2018-06-18 | Finished Plugging |
2018-09-18 | Finished Plugging |
2019-04-30 | Fully Plugged |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1986 | APOLLO GAS CO | 1,506.00 | 364 | 0.00 | 0 | 0.00 | 0 |
1987 | APOLLO GAS CO | 1,354.00 | 361 | 0.00 | 0 | 0.00 | 0 |
1988 | APOLLO GAS CO | 997.00 | 363 | 0.00 | 0 | 0.00 | 0 |
1989 | APOLLO GAS CO | 913.00 | 372 | 0.00 | 0 | 0.00 | 0 |
1991 | APOLLO GAS CO | 838.00 | 359 | 0.00 | 0 | 0.00 | 0 |
1997 | CARNEGIE PROD CO | 1363 | 365 | 0.00 | 0 | 0.00 | 0 |
1998 | CARNEGIE PROD CO | 1311 | 365 | 0.00 | 0 | 0.00 | 0 |
1999 | CARNEGIE PROD CO | 1154 | 365 | 0.00 | 0 | 0.00 | 0 |
2000 | EQUITRANS INC | 1135 | 365 | 0.00 | 0 | 0.00 | 0 |
2001 | EQUITABLE PROD EASTERN STATES EXPLORATION INC | 1238 | 365 | 0.00 | 0 | 0.00 | 0 |
2003 | EQT PROD CO | 1221 | 365 | 0.00 | 0 | 0.00 | 0 |
2004 | EQT PROD CO | 1349 | 366 | 0.00 | 0 | 0.00 | 0 |
2005 | EQT PROD CO | 1472 | 335 | 0 | 335 | 0.00 | 0 |
2006 | EQT PROD CO | 1,378.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2007 | EQT PROD CO | 1087.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2008 | EQT PROD CO | 1368.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2009 | EQT PROD CO | 1301.00 | 304 | 0.00 | 0 | 0.00 | 0 |
2010 | EQT PROD CO | 10.00 | 31 | 0.00 | 0 | 0.00 | 0 |
2011 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2014 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2015 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2016 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2017 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2018 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2617485 | Primary Facility | 2017-07-21 | Administrative/File Review | No Violations Noted | |
2715326 | Primary Facility | 2018-04-06 | Administrative/File Review | No Violations Noted | Reviewed Notice of Intent to Plug. |
2737564 | Primary Facility | 2018-06-05 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Met on site with Company Rep Al Reken. Penn Mechanical rig ran tools to approximately 2700'. EQT is planning on perforating the well with 2 shits every 200' from 2700' to 300' and setting cement plugs from td to surface. Due to the compromised integrity if the well, the 3 1/2" casing will be left in place and cemented inside and out. |
2740242 | Primary Facility | 2018-06-06 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Met on site with Company Rep Al Reken. Penn Mechanical rig ran tools again and are sitting down higher in the well. Running in 1 1/2" tubing and will pump on the tubing and flush down. HB Cementing on location to pump. |
2740244 | Primary Facility | 2018-06-07 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Met on site with Company Rep Al Reken. Penn Mechanical rig, HB Cementing, and Timco on location. Tubing set off at 2658'. Timeco able to make it to 2612'. Shot holes through 1 1/2" and 3". Shooting 2 holes every 200'. |
2741299 | Primary Facility | 2018-06-14 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Met on site with Company Rep Al Reken. Penn Mechanical rig on location. Howard Drilling on location pumping cement. Last plug was tagged at 1024'. Well is being cemented from attainable TD to surface. |
2767618 | Primary Facility | 2018-08-27 | Administrative/File Review | No Violations Noted |
For data sources see[6]