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Well ID: 37-065-26106 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Jefferson | |
Municipality: Knox Township | |
Operator Name: SNYDER BROS INC | |
Well Pad ID: | |
Farm/Lease Name: B & P 13 2 2 | |
License Status: ACTIVE | |
Spud Date: | |
Permit Date: 2007-12-31 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 41.100242 | |
Longitude: -79.088361 |
Date | Event |
---|---|
2007-12-31 | New Permit Application |
2008-02-01 | Performed Spud Operation |
2008-02-08 | Drilling Completion |
2008-10-23 | NEWLY DRILLED |
2009-02-11 | Drilling Completion |
2009-02-11 | Perforation |
2010-10-27 | REWORKED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2008 | SNYDER BROS INC | 2304.00 | 66 | 0.00 | 0 | 0.00 | 0 |
2009 | SNYDER BROS INC | 13397.00 | 268 | 0.00 | 0 | 0.00 | 0 |
2010 | SNYDER BROS INC | 13,934.00 | 345 | 0.00 | 0 | 0.00 | 0 |
2011 | SNYDER BROS INC | 12,714.00 | 316 | 0.00 | 0 | 0.00 | 0 |
2012 | SNYDER BROS INC | 10,585.00 | 331 | 0.00 | 0 | 0.00 | 0 |
2013 | SNYDER BROS INC | 8,673.00 | 304 | 0.00 | 0 | 0.00 | 0 |
2014 | SNYDER BROS INC | 7,826.00 | 318 | 0.00 | 0 | 0.00 | 0 |
2015 | SNYDER BROS INC | 6,597.00 | 301 | 0.00 | 0 | 0.00 | 0 |
2016 | SNYDER BROS INC | 5,181.00 | 334 | 0.00 | 0 | 0.00 | 0 |
2017 | SNYDER BROS INC | 1,076.00 | 266 | 0.00 | 0 | 0.00 | 0 |
2018 | SNYDER BROS INC | 3,668.00 | 309 | 0.00 | 0 | 0.00 | 0 |
2019 | SNYDER BROS INC | 3,398.00 | 303 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2009 | SNYDER BROS INC | Brine | 215.00 Bbl | Reuse other than road spreading | |
2010 | SNYDER BROS INC | Produced Fluid | 210.00 Bbl | Reuse other than road spreading | |
2010 | SNYDER BROS INC | Produced Fluid | 40.00 Bbl | ROAD SPREADING | |
2011 | SNYDER BROS INC | Produced Fluid | 75.00 Bbl | ROAD SPREADING | |
2011 | SNYDER BROS INC | Produced Fluid | 721.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0101508 |
2012 | SNYDER BROS INC | Produced Fluid | 90.00 Bbl | ROAD SPREADING | |
2012 | SNYDER BROS INC | Produced Fluid | 465.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0101508 |
2013 | SNYDER BROS INC | Produced Fluid | 70.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
2013 | SNYDER BROS INC | Produced Fluid | 416.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0101508 |
2013 | SNYDER BROS INC | Produced Fluid | 416 Bbl | CENT WASTE TRT FAC NPDES | PA0101508 |
2013 | SNYDER BROS INC | Produced Fluid | 70 Bbl | CENT WASTE TRT FAC NPDES | PA0095273 |
2014 | SNYDER BROS INC | Produced Fluid | 431.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0101508 |
2014 | SNYDER BROS INC | Produced Fluid | 115.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095443 |
2014 | SNYDER BROS INC | Produced Fluid | 115 Bbl | CENT WASTE TRT FAC NPDES | PA0095443 |
2014 | SNYDER BROS INC | Produced Fluid | 431 Bbl | CENT WASTE TRT FAC NPDES | PA0101508 |
2016 | SNYDER BROS INC | Produced Fluid | 110.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
2016 | SNYDER BROS INC | Produced Fluid | 110 Bbl | CENT WASTE TRT FAC NPDES | PA0095273 |
2016 | SNYDER BROS INC | Produced Fluid | 70.00 Bbl | Reuse other than road spreading | |
2016 | SNYDER BROS INC | Produced Fluid | 60 Bbl | CENT WASTE TRT FAC NPDES | PA0101508 |
2016 | SNYDER BROS INC | Produced Fluid | 60.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0101508 |
2017 | SNYDER BROS INC | Produced Fluid | 85.00 Bbl | REUSE (AT WELL PAD) | |
2017 | SNYDER BROS INC | Produced Fluid | 82.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
2018 | SNYDER BROS INC | Produced Fluid | 447.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
2019 | SNYDER BROS INC | Produced Fluid | 244.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
2019 | SNYDER BROS INC | Produced Fluid | 45.00 Bbl | REUSE (AT WELL PAD) |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1677814 | Primary Facility | 2008-01-15 | Routine/Complete Inspection | No Violations Noted | |
1681421 | Primary Facility | 2008-01-30 | Routine/Complete Inspection | No Violations Noted | |
1682535 | Primary Facility | 2008-02-04 | Drilling/Alteration | No Violations Noted | |
1685811 | Primary Facility | 2008-02-19 | Routine/Complete Inspection | No Violations Noted | |
1688016 | Primary Facility | 2008-02-28 | Routine/Complete Inspection | No Violations Noted | |
2082323 | Primary Facility | 2012-07-10 | Routine/Complete Inspection | No Violations Noted | |
2432034 | Primary Facility | 2015-12-10 | Routine/Complete Inspection | No Violations Noted | |
2834188 | Primary Facility | 2019-01-31 | Routine/Complete Inspection | No Violations Noted | Inspected location. Upon arrival I noticed a continuous amount of gas leaking out of the 4 1/2 x 7 inch annulus. I looked at the well records and it shows 528 feet of cemented 7" and 613 feet of 4 1/2 casing on a packer. I contacted Todd Kuselman with Snyder Brothers to let him know there maybe a casing issue. Under 78.86 requires the operator to repair the problem or to have a plan to repair the problem in 30 days. Todd was going to check previous records and documents giving the history of the well and the area ( 5 mile creek with gas bubbling in the stream years ago) to check into the issue. |
For data sources see[7]