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Well ID: 37-065-26743 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Jefferson | |
Municipality: Rose Township | |
Operator Name: DIVERSIFIED OIL & GAS LLC | |
Well Pad ID: | |
Farm/Lease Name: JOINER WH 39007 | |
License Status: | |
Spud Date: 2009-10-16 | |
Permit Date: 2009-06-08 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 41.091710 | |
Longitude: -79.1056 |
Date | Event |
---|---|
2009-06-08 | New Permit Application |
2009-10-16 | Performed Spud Operation |
2009-10-22 | Drilling Completion |
2010-07-08 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2009 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2010 | SENECA RESOURCES CO LLC | 18,960.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | SENECA RESOURCES CO LLC | 10,869.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2012 | SENECA RESOURCES CO LLC | 12,181.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2013 | SENECA RESOURCES CO LLC | 8,626.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | SENECA RESOURCES CO LLC | 6,827.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | SENECA RESOURCES CO LLC | 5,262.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | DIVERSIFIED OIL & GAS LLC | 4,918.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2017 | DIVERSIFIED OIL & GAS LLC | 3,605.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | DIVERSIFIED OIL & GAS LLC | 3,381.00 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2009 | SENECA RESOURCES CO LLC | Drilling | 540.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0101508 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1836855 | Primary Facility | 2009-10-21 | Drilling/Alteration | No Violations Noted | |
1928123 | Primary Facility | 2010-11-16 | Routine/Complete Inspection | No Violations Noted | |
2133620 | Primary Facility | 2013-01-24 | Routine/Complete Inspection | No Violations Noted | |
2797835 | Primary Facility | 2018-10-23 | Routine/Partial Inspection | No Violations Noted | This is a well located within the 2500' buffer zone for a current gas migration. At the time of inspection, the well was producing. The tubing, production, and intermediate casing valves are all open and producing. The pressure reading for the tubing was 16.1 psi, and the production casing pressure was also 16.1 psi. The intermediate casing was reading 100% methane, but no pressure was measurable.
The well was properly labeled. The well was equipped with a separator and 100 bbl plastic tank (which is contained within an earthen dike). Production reported in 2017 was 3605 mcf for 365 days. |
2812108 | Primary Facility | 2018-12-07 | Routine/Partial Inspection | No Violations Noted | At the time of inspection, well was being vented to a tank as requested by the Department. All valves were open, but the production casing is only opened about 1/2 way. This was so back pressure can be held on the well to prevent water intake from formation. Gas can be hard venting from the tank to atmosphere. |
2818550 | Primary Facility | 2018-12-19 | Routine/Partial Inspection | No Violations Noted | At the time of inspection, well is back online. The tubing valve is wide open and production casing is punched open. The annulus to production casing is being vented to atmosphere. |
2824765 | Primary Facility | 2019-01-03 | Routine/Partial Inspection | No Violations Noted | At the time of inspection, well was producing. The annuli remains vented. Inspection was done with Jeff Forsythe (a Diversified employee) and 2 other DEP employees. Gas samples were taken from the 7"-4 1/2", 4 1/2"-tubing, and inside of the tubing. Plan was to leave the annulus vented and permit production to continue for the other casings. |
For data sources see[7]