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Well ID: 37-081-21477 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Lycoming | |
Municipality: Cogan House Township | |
Operator Name: RANGE RESOURCES APPALACHIA LLC | |
Well Pad ID: | |
Farm/Lease Name: LAUREL HILL B UNIT 2H | |
License Status: | |
Spud Date: | |
Permit Date: 2014-06-24 | |
Well Type: GAS | |
Unconventional Well: Y | |
Configuration: Horizontal Well | |
Conservation: No | |
Latitude: 41.475464 | |
Longitude: -77.093761 |
Date | Event |
---|---|
2014-06-24 | New Permit Application |
2015-05-22 | Permit Renewal Application |
For data sources see[4]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2338208 | Primary Facility | 2015-01-12 | Incident- Response to Accident or Event | No Violations Noted | I arrived onsite at 11:15 while Weatherford was onsite completing (perf. and hydraulic fracture) two wells on the pad. At the time of the inspection, they were under pressure on the 16H well (081-21476). After arriving onsite I met with Zachary Subra, Randi Mathew, and JJ Magyar (all Range). Sumps were installed off the west side of the well pad and field conductivity was greater than 20,000 umhos/cm (the meter's upper detection limit). In addition, water from inside the containment toward the south side of containment was also over 20,000 umhos/cm. Elevated conductivity was also noted outside containment in this area. The containment in question is secondary containment for the upright brine and freshwater tanks. Based on the initial evidence, it appears brine from the upright tanks was released to the containment which subsequently released to the pad surface/ soils. Sample 3440216 was collected at 11:50 from a sump off the west side of the well pad (preliminary lab results attached). Impacted soils/sumps were being excavated. Vios-->16H |
2343229 | Primary Facility | 2015-02-11 | Routine/Complete Inspection | No Violations Noted | |
2358445 | Primary Facility | 2015-04-02 | Compliance Evaluation | No Violations Noted | I arrived onsite at 12:00 to follow-up on a 1/12/2015 NOV regarding a brine release on the site. At the time of the previous inspection; impacted soils and snow were removed to the extent possible and an intercept trench was installed and periodically vacuumed as needed. Conditions onsite remained frozen until fairly recently. |
For data sources see[5]