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37-083-02131

Well Details

Well ID: 37-083-02131
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Country: United States
State: Pennsylvania
County: McKean
Municipality: Sergeant Township
Operator Name: PVE OIL CORP INC
Well Pad ID:
Farm/Lease Name: PAGE PATTERSON
License Status: Plugged and Abandoned
Spud Date:
Permit Date:
Well Type: OIL
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 41.643305
Longitude: -78.664915

For data sources see[1][2][3]

Well History

Date Event
1952-10-03 Drilling Completion
2017-09-25 Begin Plugging
2017-10-04 Finished Plugging
2019-10-24 Fully Plugged
2019-10-24 Old Well

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 0.00 0 10.00 52 0.00 0
1992 3906.00 0 0.00 0 0.00 0
1996 0.00 0 11.83 52 0.00 0
1997 0.00 0 12.1 52 0.00 0
1998 0.00 0 10.9 52 0.00 0
1999 0.00 0 10.67 365 0.00 0
2014 PVE OIL CORP INC 0.00 0 0.00 0 0.00 0
2015 PVE OIL CORP INC 0.00 0 0.00 0 0.00 0
2016 PVE OIL CORP INC 0.00 0 0.00 0 0.00 0
2017 PVE OIL CORP INC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2632755 Primary Facility 2017-09-06 Routine/Complete Inspection No Violations Noted Well is being plugged by Pine View. 2" tubing was stuck so was shot off so as not to part it down the hole. 1" pour string will be run to bottom and formation cemented, then a plug will be placed at 800 ft and casing seat plug will be placed
2642466 Primary Facility 2017-10-02 Plugging(Includes Plugged/Mined Through) No Violations Noted Well is being plugged by Pine View. Tubing and rods were dropped down the hole in 1970. Rig crew phished out materials to 1800 ft and well was caved in at that point, remaining rods and tubing are stuck in the caving and clean out can proceed no farther. A 125 ft plug will be placed at 1800 to1675 and then a 50ft plug at 800 ft, then a casing seat plug at 500 ft.
2667517 Primary Facility 2017-12-05 Plugging(Includes Plugged/Mined Through) No Violations Noted
2718393 Primary Facility 2018-04-16 Routine/Complete Inspection No Violations Noted This well is plugged. No leaks detected.

For data sources see[6]

References