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Well ID: 37-083-06386 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: McKean | |
Municipality: Wetmore Township | |
Operator Name: SWEPI LP | |
Well Pad ID: | |
Farm/Lease Name: JOHNSON 21 | |
License Status: PLUGGED & ABANDONED | |
Spud Date: | |
Permit Date: | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 41.657233 | |
Longitude: -78.752267 |
Date | Event |
---|---|
2015-09-03 | Begin Plugging |
2015-09-14 | Drilling Completion |
2015-09-14 | Finished Plugging |
2015-10-07 | FULLY PLUGGED |
2018-08-30 | Begin Plugging |
2018-09-04 | Finished Plugging |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2010 | EAST RESOURCES MGMT LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | SWEPI LP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2014 | SWEPI LP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2016 | SWEPI LP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2018 | SWEPI LP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2016 | SWEPI LP | Produced Fluid | 22.50 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0101508 |
2016 | SWEPI LP | Produced Fluid | 22.5 Bbl | CENT WASTE TRT FAC NPDES | PA0101508 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2729963 | Primary Facility | 2018-05-15 | Routine/Complete Inspection | No Violations Noted | This is a plugged well that was reported as leaking. The well is bubbling around the cement plug and nothing appears to be venting from the vent. I put a plastic bag around the well and sealed it with tape to get a gas reading on the well, after 30 minutes I got 29% methane. Pennhills resources has claimed responsibility for the well but at the time the wells were to be transferred the policy,I was told, was not to transfer plugged wells. Pennhills has 30 days (5/27/2018) to get a plan together to stop the leak. |
572230 | Primary Facility | 1996-04-03 | Routine/Complete Inspection | No Violations Noted |
For data sources see[7]