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37-083-54573

Well Details

Well ID: 37-083-54573
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Country: United States
State: Pennsylvania
County: McKean
Municipality: Bradford Township
Operator Name: US ENERGY DEV CORP
Well Pad ID:
Farm/Lease Name: PIERCE 1
License Status:
Spud Date:
Permit Date: 2010-03-24
Well Type: OIL
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 41.957814
Longitude: -78.779386

For data sources see[1][2][3]

Well History

Date Event
2010-03-24 New Permit Application
2010-08-11 Performed Spud Operation
2010-08-13 Drilling Completion
2010-09-27 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2010 US ENERGY DEV CORP 2,166.39 350 304.06 350 0.00 0
2011 US ENERGY DEV CORP 1,456.55 298 111.42 298 0.00 0
2012 US ENERGY DEV CORP 625.02 269 131.09 269 0.00 0
2013 US ENERGY DEV CORP 684.27 336 28.31 336 0.00 0
2014 US ENERGY DEV CORP 424.04 357 40.42 357 0.00 0
2015 US ENERGY DEV CORP 108.88 42 4.42 42 0.00 0
2016 US ENERGY DEV CORP 20.43 4 0.00 0 0.00 0
2017 US ENERGY DEV CORP 307.81 37 5.85 34 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2010 US ENERGY DEV CORP Produced Fluid 243.06 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0102784
2011 US ENERGY DEV CORP Produced Fluid 317.04 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0102784
2012 US ENERGY DEV CORP Produced Fluid 102.96 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0102784
2013 US ENERGY DEV CORP Produced Fluid 132.31 Bbl CENT WASTE TRT FAC NPDES PA0102784
2013 US ENERGY DEV CORP Produced Fluid 132.31 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0102784
2014 US ENERGY DEV CORP Produced Fluid 341.54 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0102784
2014 US ENERGY DEV CORP Produced Fluid 341.54 Bbl CENT WASTE TRT FAC NPDES PA0102784
2015 US ENERGY DEV CORP Produced Fluid 2.15 Bbl INJECTION DISPOSAL WELL PAS2D215BWAR
2015 US ENERGY DEV CORP Produced Fluid 12.69 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0102784
2015 US ENERGY DEV CORP Produced Fluid 3.85 Bbl CENT WASTE TRT FAC NPDES PA0101508
2015 US ENERGY DEV CORP Produced Fluid 12.69 Bbl CENT WASTE TRT FAC NPDES PA0102784
2015 US ENERGY DEV CORP Produced Fluid 3.85 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0101508
2016 US ENERGY DEV CORP Produced Fluid 0.62 Bbl INJECTION DISPOSAL WELL PAS2D215BWAR
2016 US ENERGY DEV CORP Produced Fluid 4.23 Bbl REUSE OTHER THAN ROAD SPREADING
2017 US ENERGY DEV CORP Produced Fluid 2.46 Bbl INJECTION DISPOSAL WELL PAS2D215BWAR

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1904412 Primary Facility 2010-08-04 Drilling/Alteration No Violations Noted
1910972 Primary Facility 2010-08-17 Complaint Inspection Violation(s) Noted
1912387 Primary Facility 2010-08-27 Complaint Inspection Violation(s) Noted
1912398 Primary Facility 2010-08-18 Complaint Inspection No Violations Noted
1912427 Primary Facility 2010-08-23 Complaint Inspection No Violations Noted
1912429 Primary Facility 2010-08-30 Drilling/Alteration No Violations Noted
2769060 Primary Facility 2018-08-21 Incident- Response to Accident or Event Pending This inspection was conducted in response to US Energy's report to the Department that they were contacted by a nearby resident over the resident's concern that there was gas in their potable spring water.
2769147 Primary Facility 2018-08-22 Routine/Complete Inspection Violation(s) Noted
2770894 Primary Facility 2018-08-30 Follow-up Inspection Outstanding Violations - Viols Req'd This is a follow up inspection to the August 22, 2018 discovery of a brine discharge to groundwater from the Pierce lease in the vicinity of this well.
2792419 Primary Facility 2018-10-22 Follow-up Inspection Outstanding Violations - Viols Req'd This is a follow up inspection to the August 22, 2018 discovery of a brine discharge to groundwater from the Pierce lease in the vicinity of this well.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
1910972 594687 08/17/2010 2010-08-17 307CSL - Discharge of industrial waste to waters of Commonwealth without a permit. Environmental Health & Safety
1910972 594688 08/17/2010 2010-08-17 78.56(1) - Pit and tanks not constructed with sufficient capacity to contain pollutional substances. Administrative 78.56(a)
1910972 594689 08/17/2010 2010-08-17 SWMA301 - Failure to properly store, transport, process or dispose of a residual waste. Environmental Health & Safety
1912387 595035 08/27/2010 2010-08-27 401 CSL - Discharge of pollultional material to waters of Commonwealth. Environmental Health & Safety
1912387 595036 08/27/2010 2010-08-27 307CSL - Discharge of industrial waste to waters of Commonwealth without a permit. Environmental Health & Safety
1912387 595146 08/27/2010 2010-08-27 SWMA301 - Failure to properly store, transport, process or dispose of a residual waste. Environmental Health & Safety
2769147 826722 2018-08-22 CSL 307(a) Environmental Health & Safety
2769147 826723 2018-08-22 SWMA 301 Environmental Health & Safety After discovering the loss of pressure in the fluid gathering line, US Energy excavated around the risers for this well and found that the soil was soaked with production water and some oil. I arrived on site soon after their discovery and my conductivity meter indicated that the fluid's conductivi
2769147 826724 2018-08-22 78.54 Environmental Health & Safety A spring run located to the east of the potable spring appears to have also been impacted by this incident. The specific conductivity of the spring run next to the resident's garage was approximately 1000 umhos/cm.
2769147 826725 2018-08-22 SWMA 302(A) Environmental Health & Safety
2769147 826726 2018-08-22 SWMA 610(1) Environmental Health & Safety
2770894 827046 2018-08-30 CSL 307(a) Environmental Health & Safety
2770894 827047 2018-08-30 SWMA 302(A) Environmental Health & Safety
2770894 827048 2018-08-30 SWMA 610(1) Environmental Health & Safety
2770894 827049 2018-08-30 SWMA 301 Environmental Health & Safety US Energy has replaced the steel riser and a portion of the gathering line at this well. The specific conductivity of the soil in the open trench remains elevated and will continue to be monitored. Contaminated soil that has been excavated and will need to be disposed of has been temporarily stage
2770894 827050 2018-08-30 78.54 Environmental Health & Safety Elevated specific conductivity levels (>1000 umhos/cm) have been discovered in four spring runs downslope from this well. These springs will be routinely monitored.
2792419 831240 2018-10-22 CSL 307(a) Environmental Health & Safety The specific conductivity readings of the impacted springs on the hillside below this well are appreciably lower than they were at the onset of this incident. Current readings range from between 100 uS/cm to 400 uS/cm, which remain somewhat elevated.
2792419 831241 2018-10-22 SWMA 610(1) Environmental Health & Safety
2792419 831242 2018-10-22 SWMA 302(A) Environmental Health & Safety
2792419 831243 2018-10-22 78.54 Environmental Health & Safety
2792419 831244 2018-10-22 SWMA 301 Environmental Health & Safety The specific conductivity of the standing water within the open trench remains elevated (~450 uS/cm) and will continue to be monitored. A minimal amount of additional excavation from the floor of this trench should be considered before reclamation of the trench. Contaminated soil that has been exc

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
826722 367186 NOV - Notice of Violation
826723 367186 NOV - Notice of Violation
826724 367186 NOV - Notice of Violation
826725 367186 NOV - Notice of Violation
826726 367186 NOV - Notice of Violation

For data sources see[7]

References