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Well ID: 37-085-24352 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Mercer | |
Municipality: Deer Creek Township | |
Operator Name: VISTA OPR INC | |
Well Pad ID: | |
Farm/Lease Name: MCCARTNEY R 2 270 | |
License Status: ACTIVE | |
Spud Date: | |
Permit Date: 2007-11-01 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: Yes | |
Latitude: 41.4406 | |
Longitude: -80.163919 |
Date | Event |
---|---|
2007-11-01 | New Permit Application |
2007-11-12 | Performed Spud Operation |
2007-11-17 | Drilling Completion |
2007-11-28 | Perforation |
2008-02-27 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2007 | VISTA OPR INC | 3546.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2008 | VISTA OPR INC | 14834.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2009 | VISTA OPR INC | 7726.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2010 | VISTA OPR INC | 6,050.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | VISTA OPR INC | 4,727.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2012 | VISTA OPR INC | 3,678.00 | 365 | 34.70 | 365 | 0.00 | 0 |
2013 | VISTA OPR INC | 2,817.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | VISTA OPR INC | 2,220.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | VISTA OPR INC | 2,648.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | VISTA OPR INC | 2,337.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2017 | VISTA OPR INC | 2,226.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | VISTA OPR INC | 1,040.00 | 365 | 32.34 | 31 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2008 | VISTA OPR INC | Brine | 50.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0101508 |
2010 | VISTA OPR INC | Produced Fluid | 30.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0101508 |
2012 | VISTA OPR INC | Produced Fluid | 40.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0101508 |
2014 | VISTA OPR INC | Produced Fluid | 15 Bbl | CENT WASTE TRT FAC NPDES | PA0101508 |
2014 | VISTA OPR INC | Produced Fluid | 15.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0101508 |
2017 | VISTA OPR INC | Produced Fluid | 23.81 Bbl | ROAD SPREADING | |
2018 | VISTA OPR INC | Produced Fluid | 13.50 Bbl | ROAD SPREADING |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2233632 | Primary Facility | 2013-12-26 | Routine/Complete Inspection | No Violations Noted | |
2705571 | Primary Facility | 2018-03-14 | Routine/Complete Inspection | No Violations Noted | Inspected in response to complaint about a leaking well. Producing conventional gas well with rabbit and cattle guard at wellhead. Wellhead (Photo # 1) is below grade, under water (snow is melted around wellhead) and bubbling small amount of gas. Unknown exactly where gas is coming from. Tanks and separator in earthen dike. Company info also posted on 100 bbl tank. Shared tank battery with McCartney 1 (085-24347).
Referring inspection of well to Oil and Gas Inspector for follow-up. |
2707513 | Primary Facility | 2018-03-15 | Routine/Partial Inspection | No Violations Noted | Locked gate at entrance to access road. Well is about .75 - 1 mile back access road in state game lands. Well has a fence made of 1-1/2" tubing painted yellow around it. Well is located in a depression filled with water. Tubing open to separator unit. Separator unit has a weekly chart on meter with production. Production casing is shut. Surface casing valve is not visible but appears to be open to 100 bbl tank based on 1" line connected to tank. Bubbles can be seen coming from below well head up through the water.
Inspection done as the result of a complaint about a leaking oil & gas well. |
2708757 | Primary Facility | 2018-03-22 | Routine/Complete Inspection | No Violations Noted | Routine inspection to follow-up on recent work done at wellhead to correct minor gas leak. Operator exposed well casing/wellhead, tightened a hammer union that was loose, and added soil around casing to shed water away from wellhead (Photo 1).
|
2709876 | Primary Facility | 2018-03-26 | Complaint Inspection | No Violations Noted | Complaint previously closed by Mercer County WQS. Complaint was about gas leaking around wellhead. Gas no longer leaking around.
GPS coordinates taken at well with inspection app as required for complaint inspections. |
For data sources see[7]