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Well ID: 37-105-00005 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Potter | |
Municipality: Ulysses Township | |
Operator Name: ARDENT RESOURCES INC | |
Well Pad ID: | |
Farm/Lease Name: JOSEPH TOROK 1 | |
License Status: ACTIVE | |
Spud Date: | |
Permit Date: | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 41.846730 | |
Longitude: -77.829523 |
Date | Event |
---|---|
1940-01-29 | Drilling Completion |
1993-01-01 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1980 | DOMINION ENERGY TRANS INC | 15,544.00 | 0 | 0.00 | 0 | 0.00 | 0 |
1981 | DOMINION ENERGY TRANS INC | 13,790.00 | 0 | 0.00 | 0 | 0.00 | 0 |
1982 | DOMINION ENERGY TRANS INC | 11,691.00 | 0 | 0.00 | 0 | 0.00 | 0 |
1983 | DOMINION ENERGY TRANS INC | 12,419.00 | 0 | 0.00 | 0 | 0.00 | 0 |
1984 | DOMINION ENERGY TRANS INC | 13,018.00 | 0 | 0.00 | 0 | 0.00 | 0 |
1985 | DOMINION ENERGY TRANS INC | 13,901.00 | 0 | 0.00 | 0 | 0.00 | 0 |
1991 | DOMINION ENERGY TRANS INC | 13522.00 | 365 | 0.00 | 0 | 0.00 | 0 |
1993 | ARDENT RESOURCES INC | 11521.00 | 210 | 0.00 | 0 | 0.00 | 0 |
1994 | ARDENT RESOURCES INC | 11004.00 | 240 | 0.00 | 0 | 0.00 | 0 |
1995 | ARDENT RESOURCES INC | 13925.00 | 365 | 0.00 | 0 | 0.00 | 0 |
1996 | ARDENT RESOURCES INC | 13489 | 365 | 0.00 | 0 | 0.00 | 0 |
1997 | ARDENT RESOURCES INC | 11440 | 365 | 0.00 | 0 | 0.00 | 0 |
1998 | ARDENT RESOURCES INC | 5959 | 365 | 0.00 | 0 | 0.00 | 0 |
1999 | ARDENT RESOURCES INC | 2379 | 180 | 0.00 | 0 | 0.00 | 0 |
2000 | ARDENT RESOURCES INC | 2525 | 150 | 0.00 | 0 | 0.00 | 0 |
2001 | ARDENT RESOURCES INC | 279 | 30 | 0.00 | 0 | 0.00 | 0 |
2004 | ARDENT RESOURCES INC | 15525 | 269 | 0.00 | 0 | 0.00 | 0 |
2005 | ARDENT RESOURCES INC | 18086 | 365 | 0.00 | 0 | 0.00 | 0 |
2006 | ARDENT RESOURCES INC | 10503.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2007 | ARDENT RESOURCES INC | 5624.00 | 243 | 0.00 | 0 | 0.00 | 0 |
2008 | ARDENT RESOURCES INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2009 | ARDENT RESOURCES INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2010 | ARDENT RESOURCES INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | ARDENT RESOURCES INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | ARDENT RESOURCES INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2014 | ARDENT RESOURCES INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1147902 | Primary Facility | 2002-07-02 | Routine/Complete Inspection | Violation(s) Noted | |
2820519 | Primary Facility | 2018-12-24 | Routine/Complete Inspection | No Violations Noted | This well is an approximate 7"casing out of the ground (approx. 3' in length). This casing is threaded into an approximate 7" fitting threaded on both ends connected to another approximate 2' of casing with a approximately 3" welded fitting that reduces to approximately 2" and is connected to an approximate 2" production/ flow line. This line goes into a separator then out of separator and into a filter and or desiccant type small tank. Then the flow line continues out of and away from the small tank where it increases in size to approximately 5" for approximately 6' in length with a in line flow gauge ( orifice plate ) then into the ground. The top of the wellhead assembly has an approximate 3" valve with a plug threaded into it that is leaking and where combustible gas (100% lel) Lower Explosion Limit and 38% Methane was detected. (Pictures attached to this inspection show the valve with the plug that is leaking ad indicated by the icing coverage of the valve). No violations noted at this inspection. |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
1147902 | 308275 | 07/02/2002 | 2002-07-02 | 212PRODRPT - Failure to submit production report | Administrative |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
308275 | 97746 | NOV - Notice of Violation | Comply/Closed | 2002-08-12 |
For data sources see[6]