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Well ID: 37-115-20013 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Susquehanna | |
Municipality: Springville Township | |
Operator Name: CABOT OIL & GAS CORP | |
Well Pad ID: | |
Farm/Lease Name: TEEL 9 | |
License Status: | |
Spud Date: | |
Permit Date: 2007-12-03 | |
Well Type: GAS | |
Unconventional Well: Y | |
Configuration: Horizontal Well | |
Conservation: Yes | |
Latitude: 41.703325 | |
Longitude: -75.874932 |
Date | Event |
---|---|
2007-12-03 | New Permit Application |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2007 | CABOT OIL & GAS CORP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1689293 | Primary Facility | 2008-02-28 | Routine/Complete Inspection | No Violations Noted | |
1703706 | Primary Facility | 2008-04-23 | Routine/Complete Inspection | No Violations Noted | |
1703793 | Primary Facility | 2008-04-29 | Routine/Complete Inspection | No Violations Noted | |
1713874 | Primary Facility | 2008-06-03 | Routine/Complete Inspection | Violation(s) Noted | |
1716850 | Primary Facility | 2008-06-26 | Routine/Complete Inspection | Outstanding Violations - No Viols Req'd | |
1716949 | Primary Facility | 2008-06-27 | Routine/Complete Inspection | No Violations Noted | |
1723009 | Primary Facility | 2008-07-08 | Routine/Complete Inspection | No Violations Noted | |
1723066 | Primary Facility | 2008-07-16 | Routine/Complete Inspection | No Violations Noted | |
1733051 | Primary Facility | 2008-09-03 | Routine/Complete Inspection | No Violations Noted | |
2105619 | Primary Facility | 2012-09-18 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Follow up on plugging of well. Since last inspection have run a CBL and Temp Log in 7" casing. BAsed on anomalies shown on logs - have perf'd and attemted to squeeze cement to eliminate bubbling at surface. At time of inspection tripping out of hole and will be perforating later today and will see inf can establish injection rate and squeeze cement. Bubbling still present in cellar on 9 x 7" annulus. No violations observed at this time. See inspection report for perforation details. |
2110246 | Primary Facility | 2012-10-15 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Since last inspection have cut two additional windows in 7" casing at 450' and 500'. Gas bubbling at the surface has decreased substantially. Over the weekend, a cement plug was set acorss cuts from 270' to 565'. 7" was topped off with gravel and capped. At this time cellar has been backfilled to just below 9 5/8" casing. top. At the time of inspection I ovserved bubbling in 9 5/8" x 7" annulus. bubbling was sporatic - approximately 1 every 5 - 10 seconds. A welded cap is on 7" with permit #. Cellar will remain open for the next couple of weeks. Secondary containment is still in place. Rig is stacked on site along with other remaining equipment. DEP will continue to re-visit site to monitor well. |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
1713874 | 541429 | 06/03/2008 | 2008-06-03 | 102.4 - Failure to minimize accelerated erosion, implement E&S plan, maintain E&S controls. Failure to stabilize site until total site restoration under OGA Sec 206(c)(d) | Environmental Health & Safety | 102.22 & 1024b2 |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
541429 | 235099 | NOV - Notice of Violation | Comply/Closed | 2008-06-27 |
For data sources see[6]