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Well ID: 37-117-20596 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Tioga | |
Municipality: Shippen Township | |
Operator Name: SWEPI LP | |
Well Pad ID: 148495 | |
Farm/Lease Name: HAZELTON 424 1V | |
License Status: Inactive | |
Spud Date: 2010-06-11 | |
Permit Date: 2010-03-11 | |
Well Type: GAS | |
Unconventional Well: Y | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 41.702485 | |
Longitude: -77.404128 |
Date | Event |
---|---|
2010-03-11 | New Permit Application |
2010-06-10 | Performed Spud Operation |
2010-06-19 | Drilling Completion |
2011-04-29 | NEWLY DRILLED |
2016-11-09 | Inactive Well Request Granted |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2010 | EAST RESOURCES MGMT LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2011 | SWEPI LP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | SWEPI LP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | SWEPI LP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2014 | SWEPI LP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2015 | SWEPI LP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2016 | SWEPI LP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2017 | SWEPI LP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2019 | SWEPI LP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2012 | SWEPI LP | Fracing Fluid Waste | 1,071.43 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2012 | SWEPI LP | Drilling Fluid Waste | 114.29 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123 |
2012 | SWEPI LP | Fracing Fluid Waste | 75.94 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2008499 | Primary Facility | 2011-10-05 | Routine/Complete Inspection | No Violations Noted | |
2039088 | Primary Facility | 2012-01-26 | Routine/Complete Inspection | Violation(s) Noted | Applicable code not in efacts. Gas venting outside btw surface and conductor. Cited 78.81(2) - failure to prevent migration of gas or other fluides into sources of fresh groundwater. |
2049527 | Primary Facility | 2012-03-07 | Routine/Complete Inspection | No Violations Noted | |
2060115 | Primary Facility | 2012-04-17 | Routine/Complete Inspection | Outstanding Violations - No Viols Req'd | |
2132833 | Primary Facility | 2013-01-10 | Follow-up Inspection | No Violations Noted | |
2139146 | Primary Facility | 2013-02-12 | Routine/Partial Inspection | Outstanding Violations - No Viols Req'd | On 2/12/13 an inspection of the Hazelton 424 well site in Shippen Township, Tioga County was conducted. The last self-inspection conducted on behalf of the operator was on 2/5/2013 noting gurgling from the annulus. During this inspection it was noted that the pad surface was stabilized, no puddles were observed and the cut and fill slopes were well vegetated. No gurgling from the annulus was heard. A violation of §78.81(2) - failure to prevent migration of gas or other fluids into sources of fresh groundwater, cited during a 1/26/12 inspection (2039088), remains outstanding. No violations were cited during this inspection. |
2250126 | Primary Facility | 2014-02-27 | Routine/Complete Inspection | Outstanding Violations - No Viols Req'd | Presence of CG on D annulus (IR#2060115). NOV issued 4/20/12. |
2303709 | Primary Facility | 2014-09-12 | Site Restoration | No Violations Noted | Well Site Restoration Report acknowledged on 9/12/14. Well pad minimized, site permanently stabilized and temporary E&S controls removed. TLT |
2522829 | Primary Facility | 2016-09-27 | Routine/Complete Inspection | No Violations Noted | Defective surface casing cement job violation § 78.81(2), from inspection on 1/26/2012 insp record # 2039088 |
2569531 | Primary Facility | 2017-03-09 | Routine/Complete Inspection | No Violations Noted |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2039088 | 630959 | 01/26/2012 | 2012-01-26 | 78.81D2 - Failure to case and cement properly through storage reservoir or storage horizon | Administrative |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
630959 | 282805 | NOV - Notice of Violation |
For data sources see[7]