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Well ID: 37-117-20967 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Tioga | |
Municipality: Duncan Township | |
Operator Name: EQT PROD CO | |
Well Pad ID: 149047 | |
Farm/Lease Name: PHOENIX 590791 | |
License Status: | |
Spud Date: | |
Permit Date: 2010-10-15 | |
Well Type: GAS | |
Unconventional Well: Y | |
Configuration: Horizontal Well | |
Conservation: Yes | |
Latitude: 41.645314 | |
Longitude: -77.290511 |
Date | Event |
---|---|
2010-10-15 | New Permit Application |
2011-04-30 | Performed Spud Operation |
2011-07-03 | Drilling Completion |
2012-01-21 | Perforation |
2013-04-18 | DEVIATED |
For data sources see[4]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 2012-01-17 | 2012-01-17 | 6,909 | 8,905,746 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | FR-66 Friction Reducer | Halliburton Energy Services | Friction Reducer | Distillates, petroleum, hydrotreated light | 64742-47-8 | 0.03 | ||
Hydrochloric Acid | Halliburton Energy Services | Corrosion Inhibitor | Hydrochloric acid | 7647-01-0 | 0.03 | |||
Propargyl alcohol | 107-19-7 | 0.00010000 | ||||||
SP Breaker | Halliburton Energy Services | Oxidizing Breaker | Sodium persulfate | 7775-27-1 | 0.00020000 | |||
GBW-30 BREAKER | Halliburton Energy Services | Enzyme Breaker | Hemicellulase enzyme | 9012-54-8 | 0.00 | |||
BE-9 Biocide | Halliburton Energy Services | Biocide | Tri-n-butyl tetradecyl phosphonium chloride | 81741-28-8 | 0.00460000 | |||
WG-36 GELLING AGENT | Halliburton Energy Services | Gelling Agent | Guar gum | 9000-30-0 | 0.00340000 | |||
Naphtha, petroleum, hydrotreated heavy | 64742-48-9 | 0.00 | ||||||
BA-40L | Halliburton Energy Services | Buffer | Carbonic acid, dipotassium salt | 584-08-7 | 0.00004000 | |||
Hydrochloric Acid | Halliburton Energy Services | 15 HCl Acid | Methanol | 67-56-1 | 0.00030000 | |||
LP-65 | Halliburton Energy Services | Scale Inhibitor | Ammonium chloride | 12125-02-9 | 0.00280000 |
For data sources see[5]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2010 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2011 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | EQT PROD CO | 1,227,978.00 | 248 | 0.00 | 0 | 0.00 | 0 |
2013 | EQT PROD CO | 1,049,432.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | EQT PROD CO | 746,699.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | EQT PROD CO | 399,448.00 | 242 | 0.00 | 0 | 0.00 | 0 |
2016 | EQT PROD CO | 513,133.00 | 340 | 0.00 | 0 | 0.00 | 0 |
2017 | EQT PROD CO | 74,023.00 | 228 | 0.00 | 0 | 0.00 | 0 |
2018 | EQT PROD CO | 499,677.00 | 358 | 0.00 | 0 | 0.00 | 0 |
2019 | EQT PROD CO | 364,828.00 | 355 | 0.00 | 0 | 0.00 | 0 |
For data sources see[6]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2011 | EQT PROD CO | Drilling Fluid Waste | 833.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2011 | EQT PROD CO | Drilling Fluid Waste | 560.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR119 |
2011 | EQT PROD CO | Fracing Fluid Waste | 222.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR119 |
2011 | EQT PROD CO | Produced Fluid | 280.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2011 | EQT PROD CO | Fracing Fluid Waste | 7,900.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2011 | EQT PROD CO | Fracing Fluid Waste | 501.00 Bbl | INJECTION DISPOSAL WELL | 34-049-23127 |
2011 | EQT PROD CO | Drilling Fluid Waste | 400.00 Bbl | INJECTION DISPOSAL WELL | 34-049-23127 |
2012 | EQT PROD CO | Produced Fluid | 3,055.00 Bbl | INJECTION DISPOSAL WELL | 34-155-21447 |
2012 | EQT PROD CO | Produced Fluid | 14,011.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR119 |
2012 | EQT PROD CO | Produced Fluid | 1,073.00 Bbl | INJECTION DISPOSAL WELL | 34-007-24355 |
2012 | EQT PROD CO | Produced Fluid | 7,244.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123 |
2012 | EQT PROD CO | Produced Fluid | 1,000.00 Bbl | INJECTION DISPOSAL WELL | 34-155-21438 |
2012 | EQT PROD CO | Produced Fluid | 951.00 Bbl | INJECTION DISPOSAL WELL | 34-083-24137 |
2012 | EQT PROD CO | Produced Fluid | 13,610.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2012 | EQT PROD CO | Fracing Fluid Waste | 46.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123 |
2012 | EQT PROD CO | Fracing Fluid Waste | 3,171.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2012 | EQT PROD CO | Fracing Fluid Waste | 391.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR119 |
2013 | EQT PROD CO | Produced Fluid | 3,344.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2013 | EQT PROD CO | Produced Fluid | 3,081.00 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123 |
2013 | EQT PROD CO | Produced Fluid | 334.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123SW018 |
2013 | EQT PROD CO | Produced Fluid | 411.00 Bbl | INJECTION DISPOSAL WELL | 34-155-23223 |
2013 | EQT PROD CO | Produced Fluid | 5,655.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR119 |
2013 | EQT PROD CO | Produced Fluid | 1,309.00 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NC018 |
2013 | EQT PROD CO | Produced Fluid | 1,919.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123 |
2013 | EQT PROD CO | Produced Fluid | 101.00 Bbl | INJECTION DISPOSAL WELL | 34-155-21438 |
2014 | EQT PROD CO | Produced Fluid | 44.00 Bbl | INJECTION DISPOSAL WELL | 34-155-23196 |
2014 | EQT PROD CO | Produced Fluid | 1,313.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2014 | EQT PROD CO | Fracturing Fluid Waste | 0.72 Tons | LANDFILL | 101397 |
2014 | EQT PROD CO | Produced Fluid | 6,030.00 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123 |
2015 | EQT PROD CO | Produced Fluid | 100.00 Bbl | INJECTION DISPOSAL WELL | 34-007-21847 |
2015 | EQT PROD CO | Produced Fluid | 100.00 Bbl | INJECTION DISPOSAL WELL | 34-155-21893 |
2015 | EQT PROD CO | Produced Fluid | 562.00 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123 |
2015 | EQT PROD CO | Produced Fluid | 100.00 Bbl | INJECTION DISPOSAL WELL | 34-007-24355 |
2015 | EQT PROD CO | Produced Fluid | 238.00 Bbl | INJECTION DISPOSAL WELL | 34-157-25511 |
2015 | EQT PROD CO | Produced Fluid | 200.00 Bbl | INJECTION DISPOSAL WELL | 34-155-23196 |
2015 | EQT PROD CO | Produced Fluid | 2,251.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2016 | EQT PROD CO | Produced Fluid | 574.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2016 | EQT PROD CO | Produced Fluid | 714.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123NW011 |
2016 | EQT PROD CO | Produced Fluid | 653.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NW005 |
2017 | EQT PROD CO | Produced Fluid | 1,920.11 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NW011 |
2017 | EQT PROD CO | Produced Fluid | 43.33 Bbl | REUSE (AT WELL PAD) | |
2017 | EQT PROD CO | Produced Fluid | 340.20 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2017 | EQT PROD CO | Other Oil & Gas Wastes | 151.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2017 | EQT PROD CO | Produced Fluid | 45.13 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123SW005 |
2018 | EQT PROD CO | Other Oil & Gas Wastes | 18.26 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NW005 |
2018 | EQT PROD CO | Produced Fluid | 18.58 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123 |
2018 | EQT PROD CO | Produced Fluid | 831.29 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123SW005 |
2018 | EQT PROD CO | Produced Fluid | 3,687.22 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NW011 |
2018 | EQT PROD CO | Other Oil & Gas Wastes | 1.82 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NW009 |
2018 | EQT PROD CO | Produced Fluid | 256.71 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NW005 |
2018 | EQT PROD CO | Produced Fluid | 197.07 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NW009 |
2018 | EQT PROD CO | Other Oil & Gas Wastes | 36.67 Bbl | REUSE (AT WELL PAD) | |
2018 | EQT PROD CO | Produced Fluid | 287.69 Bbl | REUSE (AT WELL PAD) | |
2018 | EQT PROD CO | Other Oil & Gas Wastes | 43.63 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NW011 |
2018 | EQT PROD CO | Produced Fluid | 1,154.80 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2018 | EQT PROD CO | Other Oil & Gas Wastes | 76.55 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2019 | EQT PROD CO | Other Oil & Gas Wastes | 163.02 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2019 | EQT PROD CO | Produced Fluid | 144.02 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123 |
2019 | EQT PROD CO | Other Oil & Gas Wastes | 12.24 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123 |
2019 | EQT PROD CO | Produced Fluid | 67.51 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NW009 |
2019 | EQT PROD CO | Produced Fluid | 240.87 Bbl | REUSE (AT WELL PAD) | |
2019 | EQT PROD CO | Produced Fluid | 41.69 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123SW019 |
2019 | EQT PROD CO | Produced Fluid | 57.88 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123SW005 |
2019 | EQT PROD CO | Produced Fluid | 263.67 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NW011 |
2019 | EQT PROD CO | Produced Fluid | 1,651.47 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2019 | EQT PROD CO | Other Oil & Gas Wastes | 15.82 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NW009 |
For data sources see[7]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1979262 | Primary Facility | 2011-06-09 | Routine/Complete Inspection | No Violations Noted | |
1980685 | Primary Facility | 2011-06-15 | Drilling/Alteration | No Violations Noted | |
2007091 | Primary Facility | 2011-09-29 | Routine/Complete Inspection | No Violations Noted | |
2015174 | Primary Facility | 2011-10-28 | Routine/Complete Inspection | No Violations Noted | |
2016564 | Primary Facility | 2011-10-28 | Routine/Complete Inspection | No Violations Noted | |
2031466 | Primary Facility | 2011-12-20 | Follow-up Inspection | No Violations Noted | |
2035439 | Primary Facility | 2012-01-10 | Compliance Evaluation | No Violations Noted | |
2040558 | Primary Facility | 2012-02-01 | Routine/Complete Inspection | No Violations Noted | |
2049647 | Primary Facility | 2012-03-02 | Compliance Evaluation | No Violations Noted | |
2065699 | Primary Facility | 2012-05-01 | Compliance Evaluation | No Violations Noted | |
2092640 | Primary Facility | 2012-08-10 | Routine/Complete Inspection | No Violations Noted | Inspected wellhead only. Purpose of inspection was not to address open violations associated with pad. |
2150437 | Primary Facility | 2013-03-13 | Routine/Complete Inspection | No Violations Noted | |
2182502 | Primary Facility | 2013-07-09 | Follow-up Inspection | No Violations Noted | |
2230336 | Primary Facility | 2013-11-05 | Routine/Complete Inspection | No Violations Noted | |
2254904 | Primary Facility | 2014-02-27 | Follow-up Inspection | No Violations Noted | |
2257907 | Primary Facility | 2014-03-26 | Routine/Partial Inspection | No Violations Noted | |
2384358 | Primary Facility | 2015-06-26 | Follow-up Inspection | No Violations Noted | Follow up inspection for 2012 violations. Operator nearing end of Act 2 process. Soil confirmation sampling scheduled for 7/1/15. TLT |
2399595 | Primary Facility | 2015-08-17 | Preoperation Inspection | No Violations Noted | ESCGP was amended. Inspection to document earth work completed following amendment and prior to drilling of new wells. Disturbed areas have been stabilized and E&S controls are installed. TLT |
2485961 | Primary Facility | 2016-05-12 | Routine/Partial Inspection | No Violations Noted | Inspection to resolve outstanding violations against the Phoenix 590627 well. DEP Environmental Cleanup and Brownfield Program has approved the Act 2 final report for attainment of the Statewide Health Standards for soil at the site. As such, the 2/1/12 and 8/2/12 violations against permit #117-20725 (Phoenix 590627) are resolved. No new issues were observed at the site. TLT |
2531674 | Primary Facility | 2016-10-26 | Routine/Complete Inspection | No Violations Noted | Inspection of EQT’s Phoenix 590796 (117-20970) unconventional gas well in Duncan Twp. Tioga County conducted October 26, 2016 at 11:50 am. At the time of inspection; the well had a production tree in place, shut-in. Analog pressure gauge on the tree top was shut-in from well, 0 PSI. There was a digital scada gauge on the production casing wing valve down in the cellar; not visible. The valve for the backside of the production casing (9 5/8” x 5 ½”) annulus was partially buried at the bottom of the cellar. The valve was open at the wellhead but shut in at the vent pipe plumped to surface. The operator has plans to plug this well. There are (6) other active wells on the pad in production; #590794 (117-20969), #590792 (117-20980), #590791 (117-20967), #590790 (117-20965), #590627 (117-20725), and #590025 (117-20994). Visual inspection of WH and cellars; no obvious concerns. Went over plugging procedure for the -796 with the operator. Expected to rig up on the well next week for plugging ops. |
2533186 | Primary Facility | 2016-11-01 | Routine/Complete Inspection | No Violations Noted | Inspection of EQT’s Phoenix 590796 (117-20970) unconventional gas well in Duncan Twp. Tioga County conducted November 1, 2016 at 10:00 am. At the time of inspection; a workover rig was rigged up on the well for plugging ops. I met with the Companymen to discuss operation on the pad. Wireline was rigged up for gauge run down to the obstruction (6470’). If run is successful they’ll set the CIBP in the 5 ½” prod. csg. @ 6450’, cap with cement using dump bailer. Tomorrow they’ll circulate gel, set second CIBP (4070’), run freepoint tool and shoot off casing above freepoint (pull ~3626’ 5 ½” production casing). Allied is lined up to mix, pump, and spot (3) balanced cement plugs; #1) from the production casing stub (~3626-2526) in the 8 ½” open hole, #2) in the open hole, across the 9 5/8” shoe up into the 9 5/8” (2576-2126), and #3) (1275-1225, in the 9 5/8” csg). I plan to return Thursday when they estimate spotting balanced plugs and asked the Companymen to catch a slurry sample if I’m not on location. Aside fr |
2534409 | Primary Facility | 2016-11-03 | Routine/Complete Inspection | No Violations Noted | Inspection of EQT’s Phoenix 590796 (117-20970) unconventional gas well in Duncan Twp. Tioga County conducted November 3, 2016 at 8 am. At the time of inspection; a workover rig was rigged up on the well for plugging ops. I met with the Companymen to discuss operation on the pad since my last visit Tuesday. CIBP has been set, 6450’ with 15’ cement dump bailed; sample displayed good strength. The wireline perf’d the 4 ½” at 3850’ so the rig can establish circulation to flush mud out of the annulus to avoid the well U-tubing when they go to pull casing (heavy drilling mud on the backside of csg), and ensure casing is free. The rig couldn’t establish circulation here; went uphole w/ perfs (3650’, 3450’, 3250’) and broke circulation at 3052’.. Plans going forward; shoot & pull production casing, cement w/ Allied as scheduled for remaining balanced cmt plugs. Aside from the well being plugged there are (6) active wells on the pad in production; #590794 (117-20969), #590792 (117-20980), #590791 (117-20967), #590790 |
2545940 | Primary Facility | 2016-12-13 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Inspection of EQT’s Phoenix 590796 (117-20970) unconventional gas well in Duncan Twp. Tioga County conducted 12/13/16 at 11 am. WO Rig on location for remediation after bubbling inside the 9 5/8” was noticed after plugging ops. I met with the Companyman to discuss operations since my last visit 11/30. The rig drilled out (2) cmt plugs til they found good cmt @ ~2219. They set (2) CIBPs above that point, dump bailed 5’ cmt on top, some bubbling still reported at that point. They ran a downhole camera for which I reviewed the video on location; bubbling was definitely coming from below the bridge plugs, csg collars looked OK. At that point they circulated the hole and reportedly had no bubbling since. They set (2) more balanced cement plugs in the 9 5/8” as a precaution. The last blend they ran was 10% salt w 2% calcium chloride; samples showed good strength. No integrity issues reported on the 9 5/8”s annulus. Aside from the well being plugged there are (6) active wells on the pad in production; #590794 (117- |
2551753 | Primary Facility | 2017-01-09 | Routine/Partial Inspection | No Violations Noted | Routine partial inspection. Site snow covered. Well pad being prepared for arrival of the drill rig. Five new wells permitted and were reported as spud on 12/27/16. Entire pad surface covered by mats, which were underlain with textured liner. Crew on site working to berm up the liner around the perimeter of the pad. Impoundment 2 was frozen over and snow covered; adequate freeboard remained. Multiple piles of spoil material observed at staging area along access road. Material to be placed for subbase for the above ground storage tank pad, which will be constructed at the former Impoundment 1 location. TLT |
2592177 | Primary Facility | 2017-05-10 | Routine/Complete Inspection | No Violations Noted | I arrived on-site @11:20 hrs and met Bill Wallace of SWN. Patterson/UTI rig 294 on site, running pipe into the 593939 well, and anticipate skidding the rig to the 593940 well tonight. Site was neat, secondary containment was present and in good condition on top of rig mats. Chemical storage and backyard looked good. I departed the site @11:50 hrs. |
2614005 | Primary Facility | 2017-07-06 | Routine/Partial Inspection | No Violations Noted | No activity on the pad when I arrived. 10 K bbl. tank had been erected on the site, approximately 1/2 full of what appeared to be precipitation. Some water had collected in the pad containment near the edges; conductivity of this water was in the .45- .67 mS/cm range. The tank also appeared to have a remote monitoring system hooked up to it. Rig mats were still down over the entire pad from drilling operations. The liner berm at the site entrance seemed somewhat worn; I recommend that it be fully assessed before any fracing operations begin. |
2657491 | Primary Facility | 2017-11-01 | Incident- Response to Accident or Event | No Violations Noted | I met with Corey Giles of EQT and Neil Ketchum of Groundwater Sciences when I arrived. My inspection was in response to a reported release to the drainage ditch on the south side of the pad. A third party EHS group discovered water with elevated conductance (1-3.5 mS/cm) in the ditch on 10/31. The area had been more or less continuously vacced between the time it was discovered and the time I arrived. Corey and Neil had just finished taking soil and water conductance readings along the length of the ditch (see attached photos). Their investigation showed a gradient, beginning on the south side of the pad in the ditch approximately 100-125' east of the pad entrance, with the highest soil and water conductance in that area (6.77 mS/cm water, 2.57 mS/cm soil) and declining readings as they probed downgradient. At the time, the source of the water was unknown, but the area where the water was coming into the ditch seemed to be at the area of highest conductance. The containment berm on the pad had not yet |
2743479 | Primary Facility | 2018-06-19 | Routine/Complete Inspection | No Violations Noted | The DEP inspected the EQT – Phoenix Site C Well Pad located in Duncan Twp, Tioga Co. on 6/20/2018 @1100 hours. The weather was 78 degrees, 45% humidity and winds N 12mph. The receiving waters are listed as Sand Run (CWF) wild trout stream. The well site is in production. No activity was observed onsite during this inspection.
The site consists of the access road, freshwater impoundment, and well pad on a total of 22.4 acres. The impoundment is drawn down and almost empty. There are 11 wells currently in production, and one plugged well. The area surrounding the well pad appeared stabilized. A plastic bag containing old foam berms has blown onto the south slope of the pad and should be removed. No new violations were noted during this inspection. The following violations from Inspection Record #2657056 dated 11/01/2017, resulting from the release of a pollutional substance to the drainage ditch, remain OUTSTANDING against the PHOENIX 590627 Well (API#117-20725): 35 PS § 691.402(b) Potential to pollute |
2801208 | Primary Facility | 2018-11-07 | Routine/Complete Inspection | No Violations Noted | The DEP conducted a Routine inspection of the EQT - Phoenix Pad C located in Duncan Twp, Tioga Co. on 11/6/2018 @1115 hours. The weather was 52 degrees, rain, winds NNE13mph. No company personnel was present onsite during this inspection.
The site consists of the access road, freshwater impoundment, and well pad on a total of 22.4 acres. The impoundment is drawn down and almost empty. There are 11 wells currently capable of production, and one plugged well. The area surrounding the well pad appeared stabilized.
35 PS § 691.402(b) Potential to pollute waters of the Commonwealth 25 Pa Code 78a.57(a) Control, Storage and Disposal of Production Fluids 35 PS § 6018.301 SWMA Solid Waste Management Act The following violations from Inspection Record #2674148 dated 12/20/2017, resulting from the |
For data sources see[8]