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37-117-21297

Well Details

Well ID: 37-117-21297
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Country: United States
State: Pennsylvania
County: Tioga
Municipality: Covington Township
Operator Name: SWEPI LP
Well Pad ID: 149447
Farm/Lease Name: TORPY VAN ORDER 574 3H
License Status: INACTIVE
Spud Date:
Permit Date: 2011-07-28
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: No
Latitude: 41.719722
Longitude: -77.120481

For data sources see[1][2][3]

Well History

Date Event
2011-07-28 New Permit Application
2011-08-06 Performed Spud Operation
2011-10-06 Drilling Completion
2012-12-13 DEVIATED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2011 SWEPI LP 0.00 0 0.00 0 0.00 0
2012 SWEPI LP 0.00 0 0.00 0 0.00 0
2013 SWEPI LP 0.00 0 0.00 0 0.00 0
2014 SWEPI LP 0.00 0 0.00 0 0.00 0
2015 SWEPI LP 0.00 0 0.00 0 0.00 0
2016 SWEPI LP 0.00 0 0.00 0 0.00 0
2017 SWEPI LP 0.00 0 0.00 0 0.00 0
2019 SWEPI LP 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2008893 Primary Facility 2011-10-03 Drilling/Alteration No Violations Noted
2182059 Primary Facility 2013-07-09 Routine/Complete Inspection No Violations Noted
2501816 Primary Facility 2016-07-13 Site Restoration No Violations Noted 2 Marcellus Shale wells on this pad; 1 is plugged. Recommending approval of NOT.
2518357 Primary Facility 2016-09-12 Routine/Complete Inspection No Violations Noted Inspection of SWEPI’s Torpy & Van Order Inc 574 pad in Covington Twp, Tioga County conducted September 12, 2016 at approximately 12:00 pm. There were 2 wells on the pad at the time of inspection; the 1V (Plugged 9/7/11) and the 3H (Regulatory Inactive Status). The 1V is plugged and capped off with blanked spool with a needle valve (shut-in) on the cap. The 3H is shut in with a lower master valve and cap atop production casing spool/tubing hanger. The cellar was filled with gravel and there were (4) total vent pipes plumbed to surface coming up through the gravel. There were (2) 2” vent pipes assumed to be backside of the production casing (9 5/8” x 5 ½”) annulus. One of these vent pipes was shut-in, while the other was 90’d downward into a bucket. A field reading with an Altair 5x gas meter placed next to the vent outlet showed 100% LEL 66% Methane. The other (2) remaining smaller vent pipes I assume to be the intermediate csg’s annulus (1 ½” vent) and the surface casing’s annulus (1” vent). No gas was prese

For data sources see[6]

References