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Well ID: 37-117-21912 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Tioga | |
Municipality: Liberty Township | |
Operator Name: UNKNOWN OPR | |
Well Pad ID: | |
Farm/Lease Name: Mitstifer | |
License Status: Plugged and Abandoned | |
Spud Date: | |
Permit Date: | |
Well Type: UNDETERMINED | |
Unconventional Well: N | |
Configuration: Undetermined | |
Conservation: No | |
Latitude: 41.589179 | |
Longitude: -77.123497 |
Date | Event |
---|---|
1901-01-01 | Drilling Completion |
2019-06-20 | Old Well |
2019-10-03 | Begin Plugging |
2019-10-05 | Finished Plugging |
2020-01-14 | Fully Plugged |
For data sources see[4]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2660657 | Primary Facility | 2017-11-15 | Routine/Complete Inspection | No Violations Noted | Routine inspection of an abandoned well. 8" casing open with bucket on top. Cellar is fenced off and full of water, no bubbling was observed. No flow from inside casing was observed. |
2722511 | Primary Facility | 2018-04-20 | Routine/Complete Inspection | No Violations Noted | A routine inspection of the Mitstifer well was conducted April 20, 2018. At the time of inspection; SWN was on location along with third party slickline unit over well. Only one casing, approximately 8", was observed above ground level. The crew had a 5.9" gauge ring in the hole and reportedly tagged at 2219'. They were stuck coming out of the hole at the time of inspection. |
2743351 | Primary Facility | 2018-06-20 | Routine/Complete Inspection | No Violations Noted | A routine inspection of this abandoned well was conducted June 20, 2018. In recent months, SWN energy has built a pad, well cellar, removed part of casing, and entered wellbore for well diagnostic work in preparation of plug and abandonment. At the time of inspection, the location was vacant. The well had ~8" casing sticking up approximately 2' above ground level. The casing had a bucket over it. The cellar was partially full of fluid. No bubbling was observed. |
2775385 | Primary Facility | 2018-09-13 | Routine/Complete Inspection | No Violations Noted | A routine inspection of this abandoned well was conducted September 13, 2018. Earlier this year, SWN energy built a pad, well cellar, removed casing, and entered wellbore for well diagnostic work in preparation of plug and abandonment. At the time of inspection, The well had ~8" casing extending up from the well cellar to a point approximately 2' above ground level. The casing had a bucket over it. The cellar was partially full of fluid. No bubbling was observed. |
2834390 | Primary Facility | 2019-01-31 | Routine/Complete Inspection | No Violations Noted | A routine inspection of this abandoned legacy well was conducted January 31, 2019. SWN Production Company LLC has temporarily abandoned this well after removing casing, re-entering the well, and losing tools in the well in attempt to gather wellbore diagnostics. At the time of inspection, the location was snow-covered. The well was fenced-off and a bucket is placed over ~8" casing. The snow surrounding the well was clean; no evidence of discharge was observed. No gas was detected with an Altair 5x gas meter in the ambient air surrounding the well. No obvious major issues were observed on location during this inspection. |
For data sources see[5]