X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

37-121-01544

Well Details

Well ID: 37-121-01544
Loading map...
Country: United States
State: Pennsylvania
County: Venango
Municipality: Cranberry Township
Operator Name: VAN HAMPTON GAS & OIL CO INC
Well Pad ID:
Farm/Lease Name: JAMES SHAFFER
License Status: Plugged and Abandoned
Spud Date:
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 41.334810
Longitude: -79.658411

For data sources see[1][2][3]

Well History

Date Event
2019-05-01 Begin Plugging
2019-05-08 Finished Plugging
2019-08-16 Fully Plugged

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2010 VAN HAMPTON GAS & OIL CO INC 465.84 365 0.00 0 0.00 0
2011 VAN HAMPTON GAS & OIL CO INC 437.4 365 0.52 365 0.00 0
2012 VAN HAMPTON GAS & OIL CO INC 378.14 365 0.38 365 46.73 365
2013 VAN HAMPTON GAS & OIL CO INC 394.82 365 0.59 365 0.00 0
2014 VAN HAMPTON GAS & OIL CO INC 327.25 330 0.40 365 50.71 330
2015 VAN HAMPTON GAS & OIL CO INC 307.85 365 0.18 365 51.65 365
2016 VAN HAMPTON GAS & OIL CO INC 300.27 365 0.21 365 50.77 365
2017 VAN HAMPTON GAS & OIL CO INC 0.00 0 0.00 0 0.00 0
2018 VAN HAMPTON GAS & OIL CO INC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2014 VAN HAMPTON GAS & OIL CO INC Produced Fluid 1.76 Bbl CENT WASTE TRT FAC NPDES PA0101508
2014 VAN HAMPTON GAS & OIL CO INC Produced Fluid 1.76 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0101508
2015 VAN HAMPTON GAS & OIL CO INC Produced Fluid 0.78 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0101508
2015 VAN HAMPTON GAS & OIL CO INC Produced Fluid 0.78 Bbl CENT WASTE TRT FAC NPDES PA0101508

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1842249 Primary Facility 2009-11-05 Complaint Inspection Violation(s) Noted
1846658 Primary Facility 2009-11-24 Follow-up Inspection No Violations Noted
2596660 Primary Facility 2017-05-10 Complaint Inspection No Violations Noted
2739447 Primary Facility 2018-06-07 Routine/Partial Inspection No Violations Noted Service rig has been moved onto lease. Phone conversation with Joe Thompson with Van Hampton revealed that the rig is scheduled to set up over the well bore next week after site prep is constructed. Operator to file NOI.
2741805 Primary Facility 2018-06-15 Plugging(Includes Plugged/Mined Through) No Violations Noted Rig has been moved onto site. Operations shut down.
2744092 Primary Facility 2018-06-21 Plugging(Includes Plugged/Mined Through) No Violations Noted Inspection shows rig over the hole with operations shut down. Picture attached.
2746360 Primary Facility 2018-06-27 Plugging(Includes Plugged/Mined Through) No Violations Noted Information gathered from Joe Thompson (Van Hampton). Camera was run in the well and revealed what looks like 3/4 inch at 52 feet. Note information was not gathered on site. Operator to file NOI.
2748148 Primary Facility 2018-07-02 Plugging(Includes Plugged/Mined Through) No Violations Noted Received notice (text) from Joe Thompson on 6/29/18 that fishing operations are scheduled to start on 7/2/18 around 10:00am. Inspection shows operations shut down with no one around. Two joints of rods with fishing tool attached lying on the ground. Received text from Joe that they had to run back to the shop and returned 14:45.
2748166 Primary Facility 2018-07-03 Plugging(Includes Plugged/Mined Through) No Violations Noted Operations shut down until Friday while operator travels to WV to rent tools (via text). Fishing tools removed from the rods lying on location with an extra pup joint on site (2jnts + pup).
2750418 Primary Facility 2018-07-09 Plugging(Includes Plugged/Mined Through) No Violations Noted Operations shut down (11:15) with one joint of 1-1/2 sitting in the slips and one full joint lying on the ground along with a couple of short pup joints. Two joints of rods lying on site. Received notice that camera is scheduled to be run today between noon and one. Camera revealed 3/4 inch at 35ft. 3/4 inch is ballooned out and caused the catchall/ overshot unable to slide over pipe that was run on 7/6/18. Operator limited to tools he can run in the hole due to the 3 inch run below the Venango Sands.
2751863 Primary Facility 2018-07-13 Plugging(Includes Plugged/Mined Through) No Violations Noted Received text from Joe Thompson on 7/12/18 notifying me that they would be back over the well bore on 7/13/18 with an all-thread taper spear to try and get in the 3/4 inch. Inspection shows operations shut down.
2751988 Primary Facility 2018-07-16 Plugging(Includes Plugged/Mined Through) No Violations Noted No visible changes from inspection on 7/13/18. Operations shut down.
2753448 Primary Facility 2018-07-19 Plugging(Includes Plugged/Mined Through) No Violations Noted Operations shut down. No changes from previous inspection.
2754935 Primary Facility 2018-07-23 Plugging(Includes Plugged/Mined Through) No Violations Noted Received text from Joe Thompson that they would be back over the hole on Monday morning the 23rd. Two inch tubing was run down over the 3/4 inch. Approximately 13 ft beyond the top of the 3/4 inch at 37ft. Rig then ran an all thread spear and had no luck retrieving the 3/4 inch.
2756167 Primary Facility 2018-07-25 Plugging(Includes Plugged/Mined Through) No Violations Noted Text received 7/24/18 @ 13:03 (The men were at the rig briefly this morning. They will be back tomorrow morning.). Operations shut down.
2756969 Primary Facility 2018-07-27 Plugging(Includes Plugged/Mined Through) No Violations Noted Operations shut down. Phone conversation with Joe Thompson revealed that the rig has had no success get over the rods at 37ft. Rig will continue trying options.
2759260 Primary Facility 2018-07-31 Plugging(Includes Plugged/Mined Through) No Violations Noted Rig hands arrived at 12:30 and ran a home made tool down over the 3/4 inch at 37ft. Tool was unable to secure the rods.
2762703 Primary Facility 2018-08-08 Plugging(Includes Plugged/Mined Through) No Violations Noted Received notification from Joe Thompson that a camera is scheduled for Wednesday morning. Burkhouse Contracting on site and ran camera down hole. Pipe located at 51ft.
2763833 Primary Facility 2018-08-15 Plugging(Includes Plugged/Mined Through) No Violations Noted Operations shut down.
2767857 Primary Facility 2018-08-27 Plugging(Includes Plugged/Mined Through) No Violations Noted Spoke with Joe Thompson on 8/23/18 concerning plugging progress. Rig has been shut down the previous week due to rig hands work load. Was anticipating returning to the well on 8/24/18. Inspection shows operations shut down with no visible progress.
2768565 Primary Facility 2018-08-29 Plugging(Includes Plugged/Mined Through) No Violations Noted Information gathered on site from rig operator. Still unable to get over the 3/4inch. Currently trying to put a new collar on the 3 inch. Scheduled to try and pull the 3 inch tomorrow.
2772443 Primary Facility 2018-09-07 Plugging(Includes Plugged/Mined Through) No Violations Noted Received voice mail from Joe Thompson on 8/31/18 that they were going to try and pull the 3 inch. Inspection shows operations shut down with bottle jacks under the 3 inch. Does not appear that they were successful in pulling the 3 inch.
2773293 Primary Facility 2018-09-11 Plugging(Includes Plugged/Mined Through) No Violations Noted Operations shut down. No visible changes from previous inspection.
2778314 Primary Facility 2018-09-21 Plugging(Includes Plugged/Mined Through) No Violations Noted Operations shut down with bottle jacks under the 3 inch. Information received from Joe is that is is scheduled to meet with consultant next week.
2783238 Primary Facility 2018-10-03 Plugging(Includes Plugged/Mined Through) No Violations Noted Operations shut down. Following information gathered from Joe Thompson (text). Working on getting an overshot fabricated that will catch the collar of the 1" with a long enough barrel to swallow one joint of tubing.
2786586 Primary Facility 2018-10-10 Plugging(Includes Plugged/Mined Through) No Violations Noted Received voice mail on Oct 7, 2018 notifying me that the rigs hands would be on site Tuesday around 10am to run a home made tool. Received text Wednesday morning that a camera is scheduled to be run around 9:15. Inspection shows operations shut down at time of inspection.
2793200 Primary Facility 2018-10-23 Plugging(Includes Plugged/Mined Through) No Violations Noted Operations shut down. Joe is out of town. Requested him to contact me when he returns to discuss options.
2799359 Primary Facility 2018-11-06 Administrative/File Review No Violations Noted Meet with Joe Thompson concerning the statues of the Shaffer 95 well. Currently another home made overshot is being fabricated with a longer barrel. Joe feels confident with time that they will be able to retrieve the rods in the well bore. Work is limited due to weather and personnel.
2810616 Primary Facility 2018-12-05 Plugging(Includes Plugged/Mined Through) No Violations Noted Rig #9 set up over well. Rig crew made a catch to grab and remove 1" pipe that is at approximately 52' downhole inside of 3". 1" was caught and started coming up hole. Pipe broke loose and possibly parted. A collar from the 1" was found in the catch. Crew is going to run pipe to determine if the 1" dropped deeper.
2821721 Primary Facility 2019-01-03 Plugging(Includes Plugged/Mined Through) No Violations Noted Notified on January 2, 2019 that camera was to be run today. Camera run into well around 10 am. 3/4" pipe found at approximately 46.4'. Operator is manufacturing a tool to retrieve pipe.
2833891 Primary Facility 2019-01-30 Plugging(Includes Plugged/Mined Through) No Violations Noted Phone conversation with Joe Thompson on 1/29/19 revealed that the rig was able to retrieve the string of 3/4 inch rods. Inspection shows operations shut down due to extreme cold conditions. Photo attached shows rods pulled out (approximately 2000ft + or -).

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
1842249 575475 11/05/2009 2009-11-05 210UNPLUG - Failure to plug a well upon abandonment Administrative
1842249 575476 11/05/2009 2009-11-05 212PRODRPT - Failure to submit production report Administrative

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
575475 252386 NOV - Notice of Violation Comply/Closed 2011-05-17
575476 252386 NOV - Notice of Violation Comply/Closed 2011-05-17

For data sources see[7]

References