X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

37-123-36775

Well Details

Well ID: 37-123-36775
Loading map...
Country: United States
State: Pennsylvania
County: Warren
Municipality: Farmington Township
Operator Name: PINE RIDGE ENERGY
Well Pad ID:
Farm/Lease Name: KACZAR 4
License Status: ACTIVE
Spud Date:
Permit Date: 1985-02-04
Well Type: OIL
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 41.985021
Longitude: -79.262121

For data sources see[1][2][3]

Well History

Date Event
1985-02-04 New Permit Application
1985-03-29 Performed Spud Operation

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2001 PINE RIDGE ENERGY 0.00 0 0.00 0 0.00 0
2002 PINE RIDGE ENERGY 0.00 0 39.18 240 0.00 0
2005 PINE RIDGE ENERGY 0.00 0 2.5 285 0.00 0
2010 PINE RIDGE ENERGY 6.00 365 11.20 365 0 365
2014 PINE RIDGE ENERGY 0.9 102 4.62 102 0.03 102
2015 PINE RIDGE ENERGY 0.00 0 3.59 90 3.85 90
2016 PINE RIDGE ENERGY 0.39 75 4.08 75 0 75
2017 PINE RIDGE ENERGY 0.26 30 3.16 30 1.58 30

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2002 PINE RIDGE ENERGY Brine 40.00 Bbl Other
2010 PINE RIDGE ENERGY Produced Fluid 2.56 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0102784
2014 PINE RIDGE ENERGY Produced Fluid 3.59 Bbl ROAD SPREADING
2015 PINE RIDGE ENERGY Produced Fluid 3.85 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0101508
2016 PINE RIDGE ENERGY Produced Fluid 5.26 Bbl REUSE OTHER THAN ROAD SPREADING

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2775489 Primary Facility 2018-09-17 Routine/Complete Inspection Violation(s) Noted This well is abandoned. The jack was removed last year and the well has been venting. This well is about 140' from a house and it is venting gas and H2s at readings of 10 to 12 ppm and 100% methane at the well head. No production reports have been filed for 2017. There is no signage only a well tag that is barely legible.
2800920 Primary Facility 2018-11-08 Routine/Complete Inspection Outstanding Violations - Viols Req'd I was contacted by Brian Haner the operator by text message on Thursday 11/1/2018 and it said "Good morning this is Brian Haner. I have those jacks all hooked up and ready to go. I do not have well reports done yet. I went and bought a new computer and waiting for internet to be hooked up at my house. It will be done soon. Thanks". "Any questions give me a shout" I replied let me know when you get the production filed. He said "it will be before Monday". I ask if he had filed MIA reports and he responded "MIA?" I told him it was mechanical integrity its more paperwork you have to file every year and he replied " I will be doing that also. When I do the production".

No production has been reported at this time. This well has continuing violations. I also furnished him with the form to register his e-mail address with green port and the instructions say to e-mail it to them but he returned it with his answer to the violation so there is still no e-mail address on file for this inspections. The well has a j

764484 Primary Facility 1994-04-20 Routine/Complete Inspection Violation(s) Noted

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2775489 828041 2018-09-17 OGA3211(G) Administrative
2775489 828042 2018-09-17 OGA3220(A) Environmental Health & Safety
2775489 828043 2018-09-17 78.121(A) Administrative
2800920 833050 2018-11-08 78.121(A) Administrative
2800920 833051 2018-11-08 OGA3220(A) Environmental Health & Safety
764484 102263 04/20/1994 1994-04-20 201TAG - Failure to install, in a permanent manner, the permit number on a completed well Administrative

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
828041 367468 NOV - Notice of Violation
828042 367468 NOV - Notice of Violation
828043 367468 NOV - Notice of Violation

For data sources see[7]

References