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37-123-42525

Well Details

Well ID: 37-123-42525
Sorry, we have no imagery here.
Sorry, we have no imagery here.
Country: United States
State: Pennsylvania
County: Warren
Municipality: Deerfield Township
Operator Name: TATONKA OIL CO LLC
Well Pad ID:
Farm/Lease Name: NANCY 13
License Status: ACTIVE
Spud Date:
Permit Date: 1998-03-12
Well Type: COMB. OIL&GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: Yes
Latitude: 41.719451
Longitude: -79.406935

For data sources see[1][2][3]

Well History

Date Event
1998-03-12 New Permit Application
1998-05-10 Performed Spud Operation
1998-05-22 Drilling Completion
1998-05-26 Perforation
2001-08-06 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2008 OZ GAS LTD 0.00 0 0.00 0 0.00 0
2009 OZ GAS LTD 0.00 0 0.00 0 0.00 0
2010 OZ GAS LTD 0.00 0 0.00 0 0.00 0
2011 OZ GAS LTD 0.00 0 0.00 0 0.00 0
2012 OZ GAS LTD 0.00 0 0.00 0 0.00 0
2013 OZ GAS LTD 0.00 0 0.00 0 0.00 0
2014 OZ GAS LTD 0.00 0 0.00 0 0.00 0
2015 OZ GAS LTD 0.00 0 0.00 0 0.00 0
2016 OZ GAS LTD 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2828247 Primary Facility 2018-12-20 Follow-up Inspection No Violations Noted Well does not appear to have ever been equipped for production. Frac valve is still on production casing. Brine is leaking from a 2" nipple on production casing at a rate of approximately 1-2 gallons per day. Impacted area is approximately 20' long by 4' wide. Gas is venting from production casing annular space. There are no production lines visible on location. Access road has been water barred and de-commissioned. This well should be re-worked or plugged in the near future as the rate of leakage is likely to increase with time.
777741 Primary Facility 1998-05-21 Drilling/Alteration No Violations Noted

For data sources see[6]

References

BESbswy