If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 37-125-01583 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":40.194722,"lon":-80.363333,"icon":""}]} |
Country: United States | |
State: Pennsylvania | |
County: Washington | |
Municipality: Blaine Township | |
Operator Name: DALLAS ENERGY LLC | |
Well Pad ID: | |
Farm/Lease Name: JOSEPH LEECH 3 | |
License Status: Plugged and Abandoned | |
Spud Date: | |
Permit Date: | |
Well Type: UNDETERMINED | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.194722 | |
Longitude: -80.363333 |
Date | Event |
---|---|
1890-08-13 | Drilling Completion |
1996-08-06 | Old Well |
2016-04-26 | Begin Plugging |
2016-05-27 | Finished Plugging |
For data sources see[4]
Stimulation Date | Phase Number | Chemical Agent | Volume (gal) | Treating Pressure (psi) | Breakdown Pressure (psi) |
---|---|---|---|---|---|
0 | 0 | 0 |
For data sources see[5]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1993 | PENNZOIL PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
1996 | PENNZOIL PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
1997 | PENNZOIL PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
1998 | PENNZOIL PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
1999 | PENNZOIL PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2000 | PENNZOIL PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2001 | EAST RESOURCES INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2002 | EAST RESOURCES INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2003 | EAST RESOURCES INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2005 | EAST RESOURCES INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2006 | EAST RESOURCES INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2007 | EAST RESOURCES INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2008 | EAST RESOURCES INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2010 | EAST RESOURCES MGMT LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2011 | SWEPI LP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | SWEPI LP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | SWEPI LP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2014 | SWEPI LP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2015 | SWEPI LP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2016 | SWEPI LP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2479532 | Primary Facility | 2016-04-27 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | ConServ rigged up to begin plugging operations. |
2482022 | Primary Facility | 2016-05-03 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | ConServ waiting on water @ time of inspection. Ready to run 1" cement string to spot bottom plug. |
2482046 | Primary Facility | 2016-05-05 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | ConServ TIH w/ cement string to re-cement bottom plug. First plug totally "drank" by producing formation. |
2483667 | Primary Facility | 2016-05-11 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | ConServ set another bottom hole cement plug after last ones were taken by formation. |
2488954 | Primary Facility | 2016-05-19 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | ConServ WOC, no activity. |
2488960 | Primary Facility | 2016-05-16 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | ConServ got bottom hole plugged w/ TOC ~ 1705 feet. |
2488965 | Primary Facility | 2016-05-23 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | ConServ pumped next cement plug to ~ 700 feet, pulled string, shut down. WOC. |
2488968 | Primary Facility | 2016-05-24 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | ConServ WOC after spotting plug to ~ 700 feet. |
2488971 | Primary Facility | 2016-05-26 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | ConServ perforating 4 1/2" casing to cement to surface. A large hole in the casing @ 150 feet prevented them from attempting to pull the casing. |
2488974 | Primary Facility | 2016-05-27 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | ConServ finished plugging to surface, WOC. |
For data sources see[7]