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Well ID: 37-125-02271 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Washington | |
Municipality: Charleroi Borough | |
Operator Name: UNKNOWN OPR | |
Well Pad ID: | |
Farm/Lease Name: FALLOWFIELD | |
License Status: | |
Spud Date: | |
Permit Date: | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.142861 | |
Longitude: -79.903194 |
Date | Event |
---|---|
1901-01-01 | Drilling Completion |
2014-09-23 | OLD WELL |
For data sources see[4]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2420818 | Primary Facility | 2015-04-30 | Plugging(Includes Plugged/Mined Through) | No Adverse Event or Action Reported | Inspected location prior to Hydrocarbon moving rig onto well. Took photos. |
2420914 | Primary Facility | 2015-06-10 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | Hydrocarbon loading hole w/ fresh water, running washover shoe to clean out cement between 2 7/8" tubing and 6 5/8" casing. |
2420922 | Primary Facility | 2015-06-11 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | Hydrocarbon finished drilling down second washover shoe, clearing 40 feet of cement from between the 2 7/8" tubing and 6 5/8" casing. Will shut down until they can get casing jacks, box tap and overshot. |
2420927 | Primary Facility | 2015-06-17 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | Hydrocarbon used overshot to grab 2 7/8" tubing. Pulled tubing free w/ casing jacks and recovered ~250 feet. Tubing parted @ a bad collar. Tubing is almost completely filled w/ cement/calcite scale? |
2420934 | Primary Facility | 2015-06-18 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | Hydrocarbon TIH w/ 5 1/2" bit on tubing, set down @ 40 feet. Rigged up power swivel, repaired swivel hose. All tubing pulled so far is filled w/ calcite (?). |
2420947 | Primary Facility | 2015-06-22 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | Hydrocarbon drilling cement out of 6 5/8" casing (section that 2 7/8" tubing has been removed). Depth at time of inspection ~118 feet. |
2420964 | Primary Facility | 2015-06-23 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | Hydrocarbon drilling cement out of 6 5/8" casing, losing some circulation. Encountered a tight spot @156 feet. Drilled to 230 feet, started to mill on top of remaining 2 7/8" tubing (?). |
2420969 | Primary Facility | 2015-06-24 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | Hydrocarbon TIH w/ washover pipe, washed down 10 feet, TOOH. TIH w/ overshot, came out w/ ~ 10 feet of 2 7/8" tubing |
2420974 | Primary Facility | 2015-06-25 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | Hydrocarbon TIH w/ overshot, grabbed 2 7/8" tubing & pulled ~300 feet more tubing for a total of 541 feet so far. |
2420981 | Primary Facility | 2015-06-30 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | Hydrocarbon finished w/ washover pipe between the 2 7/8" tubing and 6 5/8" casing, TOOH, TIH w/ overshot. Will pull tubing w/ casing jacks. |
2421011 | Primary Facility | 2015-07-08 | Plugging(Includes Plugged/Mined Through) | No Adverse Event or Action Reported | Hydrocarbon shut down, WO smaller bit. Met w/ Susan Ghoweri at site to review activities to date, inspected tubing and packer retrieved from well. |
2421082 | Primary Facility | 2015-07-13 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | Hydrocarbon TIH w/ tubing & tricone bit to continue cleaning out hole. |
2421085 | Primary Facility | 2015-07-14 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | Hydrocarbon circulating rope fragments from hole to pit. Pulled up on tubing; pulling tight (rope settled around bit and tubing). |
2421088 | Primary Facility | 2015-07-21 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | Hydrocarbon drilled to 730 feet, lost all circulation. TOOH (wiper trip), TIH to 730 feet, re-established circulation. |
2421093 | Primary Facility | 2015-07-22 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | Met w/ Steve Jones (Hydrocarbon) on site to discuss new tool he had fabricated: tubing collar w/ hardened cross-ribs. Will use as adrill bit, will add turbulence to circulating cuttings and help move rope fragments up and out. Mud pump broke down while at depth of 730 feet. |
2421096 | Primary Facility | 2015-07-28 | Plugging(Includes Plugged/Mined Through) | No Adverse Event or Action Reported | Hydrocarbon delivered a replacement mud pump (waiting on parts for other pump), but it would not pump. Worked on pump. |
2421100 | Primary Facility | 2015-07-30 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | Hydrocarbon drilled down to 764 feet w/ paddle bit (photo). Pieces of rope in returns were plugging bit & hoses, so circulated, TOOH, cleaned out bit and TIH to 500 feet. Shut down, waiting on water delivery. |
2421107 | Primary Facility | 2015-08-03 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | Hydrocarbon waited on water, placed new liners in cellar and under mud pump. Finished tripping into hole w/ paddle bit, got to 720 feet. |
2421113 | Primary Facility | 2015-08-06 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | Hydrocarbon repaired blown seal on mud pump. TIH w/ mill bit to drill below 780 feet. |
2421121 | Primary Facility | 2015-08-10 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | Hydrocarbon had down-hole camera run in well, only got to 670 feet, as hole was bridged. Hole in 6 5/8" casing seen @ 211 feet. |
2421124 | Primary Facility | 2015-08-11 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | Hydrocarbon cleaned out down to 784 feet, circulating a lot of rope fragments out. Got call mid-morning from Charleroi Borough to cease operations due to funding shortfall. |
2421133 | Primary Facility | 2015-09-11 | Plugging(Includes Plugged/Mined Through) | No Adverse Event or Action Reported | Most of Hydrocarbon equipment remains on location since call by Charleroi Borough to cease operations on 8/11/15. |
2421142 | Primary Facility | 2015-10-30 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Hydrocarbon removed all equipment, cleaned, graded, seeded and mulched the site. Vent was installed on well. |
2488805 | Primary Facility | 2016-05-23 | Plugging(Includes Plugged/Mined Through) | No Adverse Event or Action Reported | Visited site to check on wellhead and vent; appeared intact. |
2512314 | Primary Facility | 2016-08-01 | Plugging(Includes Plugged/Mined Through) | No Adverse Event or Action Reported | Vent remains intact, no noticeable gas venting. adjacent water well (?) show water level 2-3 feet below ground level and is not bubbling. Site has become grown up w/ weeds. |
2614870 | Primary Facility | 2017-07-12 | Routine/Partial Inspection | In Compliance with Policy | Visited site to check vent on well. Intact, no gas noted. Site remains taped off w/ caution tape. |
2682682 | Primary Facility | 2018-01-16 | Routine/Partial Inspection | No Viols - Permanently Shut Down | Visited site to check status of well vent. Intact and functional, unchanged from last visit. Unable to determine if any gas was venting. |
2779399 | Primary Facility | 2018-09-25 | Routine/Partial Inspection | No Viols - Permanently Shut Down | Well vent remains intact and functional. Adjacent water well (?) has no water level visible. |
For data sources see[5]