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Well ID: 37-125-28361 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Washington | |
Municipality: East Finley Township | |
Operator Name: CNX GAS CO LLC | |
Well Pad ID: 152377 | |
Farm/Lease Name: CNX | |
License Status: | |
Spud Date: | |
Permit Date: 2017-10-02 | |
Well Type: GAS | |
Unconventional Well: Y | |
Configuration: Horizontal Well | |
Conservation: No | |
Latitude: 40.004321 | |
Longitude: -80.399459 |
Date | Event |
---|---|
2017-10-02 | New Permit Application |
2017-11-10 | Performed Spud Operation |
For data sources see[4]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 2018-05-28 | 2018-06-12 | 7,449 | 14,297,700 | 0 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | NME-375N | U.S. Well Services, LLC | Surfactant | Isopropyl alcohol | 67-63-0 | 50 | 0.00022394 | 317.97 |
Citrus Terpenes | 68647-72-3 | 60 | 0.000268728 | 381.563 | ||||
Silver FR 543 | Silverback Chemical | Friction Reducer | Distillates, hydrotreated light (petroleum) | 64742-47-8 | 30 | 0.0237953 | 33786.7 | |
Alcohols, C11-14-iso-, C13-rich, ethoxylated | 78330-21-9 | 5 | 0.00396589 | 5631.12 | ||||
Sand | U.S. Well Services, LLC | Proppant | Crystalline Silica, quartz | 14808-60-7 | 100 | 15.1892 | 21,567,000.0 | |
AI-303 | U.S. Well Services, LLC | Acid Corrosion Inhibitors | Ethylene glycol | 107-21-1 | 40 | 0.00006814 | 96.752 | |
Polyether | 60828-78-6 | 10 | 0.00001704 | 24.188 | ||||
Acetophenone,thiourea,formaldehyde polymer | 68527-49-1 | 5 | 0.00000852 | 12.094 | ||||
Formic acid | 64-18-6 | 20 | 0.00003407 | 48.376 | ||||
Butyl cellosolve | 111-76-2 | 20 | 0.00003407 | 48.376 | ||||
Cinnamaldehyde | 104-55-2 | 20 | 0.00003407 | 48.376 | ||||
SILVER SI 800 | Silverback Chemical | Scale Inhibitor | Water | 7732-18-5 | 80 | 0.0171889 | 24406.3 | |
Organic Phosphonyl Acid | Proprietary | 20 | 0.00429723 | 6101.59 | ||||
WFRC 2200 | U.S. Well Services, LLC | Friction Reducer | Distillates, petroleum, hydrotreated light | 64742-47-8 | 30 | 0.000363918 | 516.722 | |
Alcohols, C11-14-iso-, C13-rich, ethoxylated | 78330-21-9 | 5 | 0.00006065 | 86.12 | ||||
HCL Acid (5% to 7.5%) | U.S. Well Services, LLC | Bulk Acid | Water | 7732-18-5 | 95 | 0.622719 | 884192 | |
Hydrogen Chloride | 7647-01-0 | 7.5 | 0.049162 | 69804.6 | ||||
Bio Matar 123 | Silverback Chemical | Anti-Bacterial Agent | Glutaraldehyde | 111-30-8 | 20 | 0.00345573 | 4906.75 | |
Water | 7732-18-5 | 83 | 0.0143413 | 20363 | ||||
Quaternary ammonium compounds, benzyl-C12-16-alkyldimethyl, chlorides |
68424-85-1 | 2.5 | 0.000431966 | 613.343 | ||||
Ethanol | 64-17-5 | 30 | 0.00518359 | 7360.12 | ||||
LGC-15 | U.S. Well Services, LLC | Gelling Agents | Surfactant | 68439-51-0 | 3 | 0.00009499 | 134.869 | |
Suspending agent (solid) | 14808-60-7 | 3 | 0.00009499 | 134.869 | ||||
Petroleum Distillates | 64742-47-8 | 60 | 0.00189971 | 2697.37 | ||||
Guar Gum | 9000-30-0 | 50 | 0.00158309 | 2247.81 | ||||
AP One | U.S. Well Services, LLC | Gel Breakers | Ammonium Persulfate | 7727-54-0 | 100 | 0.00008733 | 124 | |
Water | CNX Resources | Carrier/Base Fluid | Water | 7732-18-5 | 100 | 84.0305 | 119,314,000.0 | |
LT FLUSH SYSTEM I | U.S. Well Services, LLC | Other | Mineral oil, petroleum distillates, hrdotreated light naphthenic |
64742-53-6 | 100 | 0.00161365 | 2291.2 | |
Other Chemical(s) | Listed Above | See Trade Name(s) List | Butyl cellosolve | 111-76-2 | 20 | 0.00003407 | 48.376 | |
Quaternary ammonium compounds, benzyl-C12-16-alkyldimethyl, chlorides |
68424-85-1 | 2.5 | 0.000431966 | 613.343 | ||||
Citrus Terpenes | 68647-72-3 | 60 | 0.000268728 | 381.563 | ||||
Suspending agent (solid) | 14808-60-7 | 3 | 0.00009499 | 134.869 | ||||
Cinnamaldehyde | 104-55-2 | 20 | 0.00003407 | 48.376 | ||||
Alcohols, C11-14-iso-, C13-rich, ethoxylated | 78330-21-9 | 5 | 0.00396589 | 5631.12 | ||||
Polyether | 60828-78-6 | 10 | 0.00001704 | 24.188 | ||||
Acetophenone,thiourea,formaldehyde polymer | 68527-49-1 | 5 | 0.00000852 | 12.094 | ||||
Water | 7732-18-5 | 95 | 0.622719 | 884192 | ||||
Surfactant | 68439-51-0 | 3 | 0.00009499 | 134.869 | ||||
Ethanol | 64-17-5 | 30 | 0.00518359 | 7360.12 | ||||
Organic Phosphonyl Acid | Proprietary | 20 | 0.00429723 | 6101.59 | ||||
Water | 7732-18-5 | 83 | 0.0143413 | 20363 | ||||
Petroleum Distillates | 64742-47-8 | 60 | 0.00189971 | 2697.37 | ||||
Formic acid | 64-18-6 | 20 | 0.00003407 | 48.376 | ||||
Alcohols, C11-14-iso-, C13-rich, ethoxylated | 78330-21-9 | 5 | 0.00006065 | 86.12 |
For data sources see[5]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2017 | CNX GAS CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2018 | CNX GAS CO LLC | 2,215,051.41 | 116 | 0.00 | 0 | 0.00 | 0 |
2019 | CNX GAS CO LLC | 3,370,064.12 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[6]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2018 | CNX GAS CO LLC | Drill Cuttings | 1,246.60 Tons | LANDFILL | 100172 |
2018 | CNX GAS CO LLC | Drilling Fluid Waste | 620.57 Bbl | RESIDUAL WASTE PROCESSING FACILITY | |
2018 | CNX GAS CO LLC | Soil Contaminated by Oil | 117.41 Tons | LANDFILL | CID # 28726 |
2018 | CNX GAS CO LLC | Produced Fluid | 6,790.43 Bbl | REUSE (AT WELL PAD) | |
2018 | CNX GAS CO LLC | Drilling Fluid Waste | 954.28 Bbl | SURFACE IMPOUNDMENT | 95-7-37312-19 |
2018 | CNX GAS CO LLC | Drill Cuttings | 47.74 Tons | LANDFILL | 06-08438 |
2018 | CNX GAS CO LLC | Produced Fluid | 139.14 Bbl | SURFACE IMPOUNDMENT | 95-7-37312-21 |
2018 | CNX GAS CO LLC | Other Oil & Gas Wastes | 134.29 Bbl | REUSE (AT WELL PAD) | |
2018 | CNX GAS CO LLC | Produced Fluid | 4,084.00 Bbl | SURFACE IMPOUNDMENT | 95-7-37312-19 |
2018 | CNX GAS CO LLC | Soil Contaminated by Oil | 0.06 Tons | RESIDUAL WASTE PROCESSING FACILITY | ORDER 2016-29 |
2018 | CNX GAS CO LLC | Other Oil & Gas Wastes | 94.29 Bbl | RESIDUAL WASTE PROCESSING FACILITY | ODNR 2015-29 |
2018 | CNX GAS CO LLC | Other Oil & Gas Wastes | 15.72 Bbl | RESIDUAL WASTE PROCESSING FACILITY | |
2018 | CNX GAS CO LLC | Produced Fluid | 125.00 Bbl | SURFACE IMPOUNDMENT | 95-7-37312-17 |
2018 | CNX GAS CO LLC | Filter Socks | 0.40 Tons | RESIDUAL WASTE PROCESSING FACILITY | 2014-541 |
2018 | CNX GAS CO LLC | Produced Fluid | 2,438.57 Bbl | RESIDUAL WASTE PROCESSING FACILITY | ODNR 2015-29 |
2018 | CNX GAS CO LLC | Drill Cuttings | 4.87 Tons | LANDFILL | 100277 |
2018 | CNX GAS CO LLC | Other Oil & Gas Wastes | 272.57 Bbl | SURFACE IMPOUNDMENT | 95-7-37312-19 |
2018 | CNX GAS CO LLC | Other Oil & Gas Wastes | 92.86 Bbl | SURFACE IMPOUNDMENT | 95-7-37312-21 |
2018 | CNX GAS CO LLC | Produced Fluid | 210.14 Bbl | RESIDUAL WASTE PROCESSING FACILITY | |
2018 | CNX GAS CO LLC | Other Oil & Gas Wastes | 4.29 Bbl | REUSE AT A WELL PAD OUTSIDE PENNSYLVANIA | |
2018 | CNX GAS CO LLC | Drill Cuttings | 2.47 Tons | LANDFILL | 100663 |
2018 | CNX GAS CO LLC | Waste Water Treatment Sludge | 12.66 Tons | RESIDUAL WASTE PROCESSING FACILITY | 2014-541 |
2018 | CNX GAS CO LLC | Soil Contaminated by Oil & Gas Related Spills | 117.41 Tons | LANDFILL | CID # 28726 |
2018 | CNX GAS CO LLC | Produced Fluid | 88.85 Tons | RESIDUAL WASTE PROCESSING FACILITY | 2014-541 |
2018 | CNX GAS CO LLC | Produced Fluid | 530.41 Bbl | RESIDUAL WASTE PROCESSING FACILITY | ORDER 2016-29 |
2018 | CNX GAS CO LLC | Soil Contaminated by Oil & Gas Related Spills | 0.06 Tons | RESIDUAL WASTE PROCESSING FACILITY | ORDER 2016-29 |
2018 | CNX GAS CO LLC | Drilling Fluid Waste | 255.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | ORDER 2016-29 |
2018 | CNX GAS CO LLC | Other Oil & Gas Wastes | 9.29 Bbl | RESIDUAL WASTE PROCESSING FACILITY | ORDER 2016-29 |
2018 | CNX GAS CO LLC | Drilling Fluid Waste | 47.14 Bbl | REUSE (AT WELL PAD) | |
2018 | CNX GAS CO LLC | Drilling Fluid Waste | 1,122.85 Bbl | RESIDUAL WASTE PROCESSING FACILITY | ODNR 2015-29 |
2018 | CNX GAS CO LLC | Other Oil & Gas Wastes | 30.00 Bbl | SURFACE IMPOUNDMENT | 95-7-37312-17 |
2018 | CNX GAS CO LLC | Synthetic Liner Materials | 6.14 Tons | LANDFILL | 100172 |
2019 | CNX GAS CO LLC | Produced Fluid | 944.29 Bbl | SURFACE IMPOUNDMENT | 95-7-37312-19 |
2019 | CNX GAS CO LLC | Other Oil & Gas Wastes | 17.14 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123SW005 |
2019 | CNX GAS CO LLC | Other Oil & Gas Wastes | 4.29 Bbl | RESIDUAL WASTE PROCESSING FACILITY | |
2019 | CNX GAS CO LLC | Produced Fluid | 686.57 Bbl | SURFACE IMPOUNDMENT | 95-7-37312-21 |
2019 | CNX GAS CO LLC | Other Oil & Gas Wastes | 282.14 Bbl | SURFACE IMPOUNDMENT | 95-7-37312-19 |
2019 | CNX GAS CO LLC | Produced Fluid | 217.00 Bbl | SURFACE IMPOUNDMENT | 95-7-37312-17 |
2019 | CNX GAS CO LLC | Other Oil & Gas Wastes | 12.86 Bbl | RESIDUAL WASTE PROCESSING FACILITY | ORDER 2016-29 |
2019 | CNX GAS CO LLC | Produced Fluid | 3,237.28 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123SW005 |
2019 | CNX GAS CO LLC | Produced Fluid | 1,825.95 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123SW019 |
2019 | CNX GAS CO LLC | Other Oil & Gas Wastes | 4.29 Bbl | REUSE (AT WELL PAD) | |
2019 | CNX GAS CO LLC | Other Oil & Gas Wastes | 36.00 Bbl | SURFACE IMPOUNDMENT | 95-7-37312-17 |
2019 | CNX GAS CO LLC | Produced Fluid | 13.57 Bbl | RESIDUAL WASTE PROCESSING FACILITY | |
2019 | CNX GAS CO LLC | Produced Fluid | 7,009.15 Bbl | REUSE (AT WELL PAD) | |
2019 | CNX GAS CO LLC | Other Oil & Gas Wastes | 47.72 Bbl | SURFACE IMPOUNDMENT | 95-7-37312-21 |
2019 | CNX GAS CO LLC | Produced Fluid | 263.57 Bbl | INJECTION DISPOSAL WELL | 34-157-25511 |
2019 | CNX GAS CO LLC | Produced Fluid | 5,637.16 Bbl | REUSE AT A WELL PAD OUTSIDE PENNSYLVANIA |
For data sources see[7]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2633290 | Primary Facility | 2017-08-22 | Routine/Complete Inspection | No Violations Noted | On August 22, 2017, the Department performed an inspection of the CNX MOR 31 well pad site. Present at time of inspection was Dave Fredericks (CNX). The site is located in East Finley Twp., Washington Co. The inspection was a compliance evaluation inspection related to violations noted on 7/26/17.
The operator has repaired the failed E&E BMPs and has remediated and recovered soils which had left the LOD. The operator is finishing construction of the well pad and access road. All the perimeter E&S BMPs are in place and are functional. The operator has asked to make a minor modification to the ESCGP2 permit to expand the excess soil stockpile. The minor modification was reviewed and approved by the Department in the field. 6 wells have been permitted for the site. Site is still under construction so none of the wells have been drilled. |
2640551 | Primary Facility | 2017-09-18 | Preoperation Inspection | No Violations Noted | On September 18, 2017, the Department performed an inspection of the CNX MOR31 well pad site. Present at time of inspection was Dave Frederick and Alex Molnar (CNX). The inspection was a routine inspection during construction of the site related to a request by the operator for a pre-operational inspection of the site prior to the start of drilling activity.
The operator has installed all the perimeter E&S BMPs which are in good condition. The operator has completed construction of the access road and well pad. The operator has stabilized the well pad fill slopes and site with hydro seeding. The operator was stoning the well pad and installing cellar tech well cellars at time of inspection.
|
2661834 | Primary Facility | 2017-11-16 | Drilling/Alteration | No Violations Noted | Operator reports 100' of 26" csg cemented to surface as conductor casing. Location inspection shows no apparent violations. NOVIO |
2682559 | Primary Facility | 2018-01-04 | Drilling/Alteration | No Violations Noted | Patterson 801 skidding to J well, anticipating TTR Wednesday AM. NOVIO |
2682822 | Primary Facility | 2018-01-11 | Drilling/Alteration | No Violations Noted | Operator reports 349' of 18 5/8" csg set with 25 bbls cmt returned to surface. NOVIO |
2682829 | Primary Facility | 2018-01-13 | Drilling/Alteration | No Violations Noted | Operator reports 1020' of 13 3/8" csg set with 20 bbls cmt circulated to surface. NOVIO |
2740978 | Primary Facility | 2018-06-13 | Drilling/Alteration | No Violations Noted | Operator currently fracing all 7 wells. 180 of 325 stages completed. G, K, H, and J wells completed, F, N and P wells currently being rigged up. Operator showed independent annular monitoring on each well during fracturing to ensure unwanted communication detection. Operator promised to email copy of data file showing monitoring during actual job. On site inspection showed no apparent violations. NOVIO |
2753861 | Primary Facility | 2018-07-19 | Drilling/Alteration | No Violations Noted | Operator has replaced equipment and containment since recent well site fire and expects to move frac back on location in approx. five days to resume and finish fracing operations. On site inspection showed no apparent violation. NOVIO |
2755430 | Primary Facility | 2018-07-11 | Routine/Complete Inspection | No Violations Noted | On July 11, 2018, the Department performed an inspection of the CNX, MOR31 well pad site. The site is located in East Finley Twp., Washington Co. The inspection was an compliance evaluation inspection related to a reported CNX fire and fluid release during hydraulic fracturing operations on June 27, 2018
The fire was first reported at approximately 9:30 PM Wednesday, 27 June, by the operator. Fire was reported to West Finley Fire Department, and was extinguished by approximately 12:30 AM Thursday 28 June. Initial reports indicated 7 pump trucks, a man lift, a 4000 Gallon diesel fuel truck and two acid tractor trailers (believed to be 5000 gal tanks carrying approx. 4000 gal of 28% HCl acid each) and a safety shower trailer were involved and damaged by fire. Frac crew was pumping stage 16 of 48 on the MOR31F well (125-28269) when the fire broke out. The Operator is continuing a root cause analysis of the fire and will inform the Department of those results as soon as they are available. The operator h |
For data sources see[8]