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Well ID: 37-125-28571 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Washington | |
Municipality: South Strabane Township | |
Operator Name: RANGE RESOURCES APPALACHIA LLC | |
Well Pad ID: 153759 | |
Farm/Lease Name: MUNCE WILLIAM 10060 12H | |
License Status: | |
Spud Date: | |
Permit Date: 2018-05-29 | |
Well Type: GAS | |
Unconventional Well: Y | |
Configuration: Horizontal Well | |
Conservation: Yes | |
Latitude: 40.197581 | |
Longitude: -80.189806 |
Date | Event |
---|---|
2018-05-29 | New Permit Application |
2019-05-15 | Permit Renewal Application |
For data sources see[4]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2749427 | Primary Facility | 2018-06-19 | Compliance Evaluation | No Violations Noted | On 6/14/2018, a follow up inspection was conducted in response to an operator reported spill (CTS ID: 334975), the following was observed:
>>Three roll off boxes remained on site at the time of inspection in the immediate vicinity of the area of the spill. The excavation for the spill cleanup remained open and was partially filled with water. Field testing of the water indicated normal ground water conductivity between 300-500µS. Cleanup appears to be in compliance with policy. No violation. |
2753838 | Primary Facility | 2018-07-18 | Routine/Partial Inspection | In Compliance with Policy | On 7/16/2018 at 1712, a spill was reported to the PA DEP hotline by Range Resources which had occurred at 1600 on 7/16/2018. On 7/18/2018 at approximately 0930, I conducted an incident response inspection. I met with Nicholas Reda (Range Resources) to discuss the incident and associated remediation.
Approximately 10 gallons of produced water were released to the graveled well pad under previously set containment. The cause of the release remains unknown. Specialized Professional Services Inc. (SPSI) responded and remediated the impacted area placing it into one roll-off box. The wells on site were clearly marked and within secondary containment. The production fluid/condensate tanks were within secondary containment and appeared to be in good condition. The GPUs on site appeared to be in good condition and had secondary containment. The spill was addressed in compliance with the spill policy. |
2825861 | Primary Facility | 2019-01-11 | Compliance Evaluation | No Violations Noted | On 1/11/19 a compliance evaluation inspection of the Munce Site was conducted in response to violations noted on 6/14/18. The following was observed:
>>No residual impact was found in the area of the spill. >>The site was found to be in good condition with no violations found. >>Minimal activity was viewed on site at the time of inspection. |
For data sources see[5]