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Well ID: 37-129-20222 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Westmoreland | |
Municipality: Lower Burrell City | |
Operator Name: ALLIANCE PETRO CO LLC | |
Well Pad ID: | |
Farm/Lease Name: A A LESLIE 2 | |
License Status: ACTIVE | |
Spud Date: | |
Permit Date: 1960-08-01 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.580056 | |
Longitude: -79.7060 |
Date | Event |
---|---|
1960-08-26 | Drilling Completion |
1998-11-09 | REWORKED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1991 | PEOPLES TWP LLC | 4612.00 | 12 | 0.00 | 0 | 0.00 | 0 |
1992 | PEOPLES TWP LLC | 3339.00 | 15 | 0.00 | 0 | 0.00 | 0 |
1993 | PEOPLES TWP LLC | 6382.00 | 38 | 0.00 | 0 | 0.00 | 0 |
1994 | PEOPLES TWP LLC | 5675.00 | 44 | 0.00 | 0 | 0.00 | 0 |
1995 | PEOPLES TWP LLC | 6930.00 | 41 | 0.00 | 0 | 0.00 | 0 |
1996 | PEOPLES TWP LLC | 4204 | 365 | 0.00 | 0 | 0.00 | 0 |
1997 | PEOPLES TWP LLC | 3662 | 28 | 0.00 | 0 | 0.00 | 0 |
1998 | PEOPLES TWP LLC | 1547 | 11 | 0.00 | 0 | 0.00 | 0 |
1999 | PEOPLES TWP LLC | 1908 | 6 | 0.00 | 0 | 0.00 | 0 |
2000 | PEOPLES TWP LLC | 1416 | 7 | 0.00 | 0 | 0.00 | 0 |
2001 | PEOPLES TWP LLC | 911 | 7 | 0.00 | 0 | 0.00 | 0 |
2002 | PEOPLES TWP LLC | 370 | 2 | 0.00 | 0 | 0.00 | 0 |
2004 | PEOPLES TWP LLC | 968 | 7 | 0.00 | 0 | 0.00 | 0 |
2005 | PEOPLES TWP LLC | 361 | 2 | 0.00 | 0 | 0.00 | 0 |
2006 | TW PHILLIPS GAS SUPPLY CORP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2007 | TW PHILLIPS GAS SUPPLY CORP | 1016.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2008 | TW PHILLIPS GAS SUPPLY CORP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2010 | TW PHILLIPS GAS SUPPLY CORP | 5,650.00 | 70 | 0.00 | 0 | 0.00 | 0 |
2011 | TW PHILLIPS GAS SUPPLY CORP | 9,295.00 | 363 | 0.00 | 0 | 0.00 | 0 |
2012 | XTO ENERGY INC | 8,257.00 | 366 | 0.00 | 0 | 0.00 | 0 |
2013 | XTO ENERGY INC | 4,666.00 | 326 | 0.00 | 0 | 0.00 | 0 |
2014 | XTO ENERGY INC | 3,909.00 | 282 | 0.00 | 0 | 0.00 | 0 |
2015 | XTO ENERGY INC | 3,437.21 | 340 | 0.00 | 0 | 0.00 | 0 |
2016 | XTO ENERGY INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2017 | ALLIANCE PETRO CO LLC | 4,084.00 | 334 | 0.00 | 0 | 0.00 | 0 |
2018 | ALLIANCE PETRO CO LLC | 5,089.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2019 | ALLIANCE PETRO CO LLC | 4,460.00 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2011 | TW PHILLIPS GAS SUPPLY CORP | Produced Fluid | 1.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095273 |
2018 | ALLIANCE PETRO CO LLC | Produced Fluid | 7.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2399824 | Primary Facility | 2015-08-18 | Complaint Inspection | No Violations Noted | Well operating and properly identified. |
2423611 | Primary Facility | 2015-11-02 | Routine/Complete Inspection | No Violations Noted | Well site located along PA 56. At the time of inspection well appears equipped for production. Site permanently stabilized. No E&S issues in relation to site and/or access road. Well tag present and affixed in a permanent manner. Brine tank located on site and appears to be structurally sound. |
2522621 | Primary Facility | 2016-09-27 | Routine/Complete Inspection | Pending | Well tagged and shut in until leak at purchase meter is fixed. 7" well head casing looked ok but 2" well head production tubing is badly corroded. Contacted operator and met well tender on site to request repairs to well production tubing in order to maintain the mechanical integrity of the well. Followup inspection pending. 1000 gallon plastic tank looked ok. |
For data sources see[7]