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Well ID: 37-129-23514 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Westmoreland | |
Municipality: Murrysville Borough | |
Operator Name: DAKOTA OIL & GAS CO | |
Well Pad ID: | |
Farm/Lease Name: FUGUNT | |
License Status: ACTIVE | |
Spud Date: | |
Permit Date: 1992-06-25 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.518349 | |
Longitude: -79.700590 |
Date | Event |
---|---|
1992-06-25 | New Permit Application |
1992-07-07 | Performed Spud Operation |
1992-08-03 | Drilling Completion |
1993-01-01 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1994 | PENNECO OIL CO INC | 5930.00 | 365 | 35.22 | 365 | 0.00 | 0 |
1995 | PENNECO OIL CO INC | 5007.00 | 365 | 0.00 | 0 | 0.00 | 0 |
1996 | PENNECO OIL CO INC | 4371 | 365 | 0.00 | 0 | 0.00 | 0 |
1997 | PENNECO OIL CO INC | 3660 | 365 | 0.00 | 0 | 0.00 | 0 |
1998 | PENNECO OIL CO INC | 3420 | 365 | 0.00 | 0 | 0.00 | 0 |
1999 | PENNECO OIL CO INC | 2742 | 365 | 31 | 365 | 0.00 | 0 |
2000 | PENNECO OIL CO INC | 2768 | 365 | 0.00 | 0 | 0.00 | 0 |
2001 | PENNECO OIL CO INC | 2299 | 366 | 35 | 366 | 0.00 | 0 |
2002 | PENNECO OIL CO INC | 2130 | 365 | 0.00 | 0 | 0.00 | 0 |
2003 | PENNECO OIL CO INC | 2426 | 365 | 11 | 365 | 0.00 | 0 |
2004 | PENNECO OIL CO INC | 2240 | 365 | 5.2 | 365 | 0.00 | 0 |
2005 | PENNECO OIL CO INC | 2058 | 365 | 0.00 | 0 | 0.00 | 0 |
2006 | PENNECO OIL CO INC | 1727.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2007 | PENNECO OIL CO INC | 1382.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2008 | PENNECO OIL CO INC | 1200.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2009 | PENNECO OIL CO INC | 1488.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2010 | PENNECO OIL CO INC | 1,251.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | PENNECO OIL CO INC | 923.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2012 | PENNECO OIL CO INC | 1,189.00 | 335 | 0.00 | 0 | 0.00 | 0 |
2013 | PENNECO OIL CO INC | 1,648.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | PENNECO OIL CO INC | 1,686.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | DAKOTA OIL & GAS CO | 1,455.50 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | DAKOTA OIL & GAS CO | 1,583.89 | 366 | 0.00 | 0 | 0.00 | 0 |
2017 | DAKOTA OIL & GAS CO | 1,508.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | DAKOTA OIL & GAS CO | 1,366.01 | 365 | 0.00 | 0 | 0.00 | 0 |
2019 | DAKOTA OIL & GAS CO | 1,466.40 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2014 | PENNECO OIL CO INC | Produced Fluid | 55 Bbl | CENT WASTE TRT FAC NPDES | PA0095443 |
2014 | PENNECO OIL CO INC | Produced Fluid | 55.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095443 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2257878 | Primary Facility | 2014-03-31 | Incident- Response to Accident or Event | Violation(s) Noted | Inspection in response to a spill report during nonworking hours. The Operator reported a 20 barrel brine and oil spill on Sunday 3/30/2014 @ 20:26. The Department notes that the report is within accordance the current spill policy. During the site inspection the Department observed an area approximately 80' x80' of disturbed area from the excavation of contaminated soil from the aforementioned spill. The Operator indicated that the spill was a result of possible vandalism. The spill originated at the tank valve which was previously found open. The Open valve appeared to spill approximately 20 barrels of brine and approximately 5 barrels of crude oil. The Department also observed two area of oil contaminated soil leading toward a steep hillside. The Department followed these two areas to their termination point approximately 60' down the hillside. The Operator immediately responded to the spill and hired McCutcheon Enterprises to assist with clean up. |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2257878 | 694335 | 03/31/2014 | 2014-03-31 | 78.57 - Failure to post pit approval number | Administrative | produced fluid spill |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
694335 | 310328 | NOV - Notice of Violation |
For data sources see[7]