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Well ID: 37-129-25012 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Westmoreland | |
Municipality: South Huntingdon Township | |
Operator Name: RANGE RESOURCES APPALACHIA LLC | |
Well Pad ID: 147259 | |
Farm/Lease Name: STAHL E | |
License Status: Plugged and Abandoned | |
Spud Date: 2003-09-06 | |
Permit Date: 2003-04-23 | |
Well Type: COMB. OIL&GAS | |
Unconventional Well: Y | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.156023 | |
Longitude: -79.723396 |
Date | Event |
---|---|
2003-04-23 | New Permit Application |
2003-09-06 | Performed Spud Operation |
2003-09-08 | Drilling Completion |
2004-02-27 | Newly Drilled |
2006-10-20 | New Permit Application |
2007-10-22 | New Permit Application |
2008-10-06 | Drilling Completion |
2008-10-17 | Perforation |
2008-10-27 | Performed Stimulation |
2009-08-14 | Drilled Deeper |
2017-08-22 | Begin Plugging |
2017-09-30 | Finished Plugging |
For data sources see[4]
Stimulation Date | Phase Number | Chemical Agent | Volume (gal) | Treating Pressure (psi) | Breakdown Pressure (psi) |
---|---|---|---|---|---|
2008-10-27 | Sand | 0 | 0 | 0 |
For data sources see[5]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2003 | RANGE RESOURCES APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2004 | RANGE RESOURCES APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2005 | RANGE RESOURCES APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2006 | RANGE RESOURCES APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2007 | RANGE RESOURCES APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2008 | RANGE RESOURCES APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2009 | RANGE RESOURCES APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2010 | RANGE RESOURCES APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2011 | RANGE RESOURCES APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | RANGE RESOURCES APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | RANGE RESOURCES APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2014 | RANGE RESOURCES APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2015 | RANGE RESOURCES APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2016 | RANGE RESOURCES APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2017 | RANGE RESOURCES APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[6]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2008 | RANGE RESOURCES APPALACHIA LLC | Fracking Fluid | 439.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0101508 |
2008 | RANGE RESOURCES APPALACHIA LLC | Drilling | 191.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0101508 |
2008 | RANGE RESOURCES APPALACHIA LLC | Drilling | 85.00 Bbl | Other | |
2008 | RANGE RESOURCES APPALACHIA LLC | Drilling | 520.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0091472 |
2008 | RANGE RESOURCES APPALACHIA LLC | Fracking Fluid | 2,059.00 Bbl | Municipal Sewage Treatment Plant | PA0026034 |
2008 | RANGE RESOURCES APPALACHIA LLC | Fracking Fluid | 1,866.00 Bbl | Other | |
2009 | RANGE RESOURCES APPALACHIA LLC | Drilling | 2,131.00 Bbl | Other |
For data sources see[7]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1447914 | Primary Facility | 2005-05-09 | Site Restoration | Violation(s) Noted | drill complete - not equipped within 60 days/no tag/E&S site |
1485518 | Primary Facility | 2005-10-06 | Compliance Evaluation | No Violations Noted | not equipped - inactive status requested/tag ok/E&S ok |
1822263 | Primary Facility | 2009-08-21 | Site Restoration | No Violations Noted | Performed a restoration inspection to evaluate the site in relation to the well site restoration extension request that was received by the department. Drilling completed 10/5/2008, but not in production. There are no signs of erosion and sedimentation on the well site or access road. The vegetative cover is at approximately 40% at the time of the inspection. As per the one on one conversation with Jeremy Matinko any bare spots should be reseeded and mulched to establish the min 70% coverage to complete restoration. The 6 month extension that was requested has been approved with a final restoration date of 1/5/2010. |
2113185 | Primary Facility | 2012-10-18 | Routine/Complete Inspection | Violation(s) Noted | Vertical Marcellus-129-25012 E. Stahl, Well was drilled in 2003 to the depth of 3800' , with out being active. In 2008 well was drilled deeper to the marcellus, without any activity to present date. |
2628955 | Primary Facility | 2017-08-24 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Flaring well to get ready to plug. |
2633300 | Primary Facility | 2017-09-07 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | 8/28/17 Bottom plug set @ 7861' to 7328', 38.08 sks cmt.
8/30/17 thru 8/31/17 thru 9/5/17 4.5" csg cut 5120' 5000' 4800' still not able to pull. 9/7/17 perforating two shots every 100' from 4800' to 3500'. Going to put cmt plug from 5120' to 3500'. |
2634119 | Primary Facility | 2017-09-08 | Incident- Response to Accident or Event | In Compliance with Policy | Inspection in response to a spill reported by the Operator on 9/7/2017 at 8:57pm. At the time of inspection, the Operator was actively plugging the well. The E&S plan was on site. The PPC was on site. The drill rig was placed on three feet of fill material, which appeared to be built on top of the containment. The Operator indicate that drill rid needed to be elevated due to the height of the well head. Two open top tanks and one enclosed frac tank located on site. Both open top tanks appeared to have the required 2 feet of freeboard. The Department observed two seeps adjacent to the well pad. The seeps appear to be at or near the elevation of the well pad. The material above the seeps appeared to the fill material the rig is placed on. Seep #1 and Seep #2 are identified in the attached photos. The Operator indicated that the release occurred while the rig was circulating fresh water in the production casing, which over filled the cellar with water. The Operator indicated that the water was sourced from a f |
2635566 | Primary Facility | 2017-09-13 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | 8/28/17 Bottom plug set @ 7861' to 7328', 38.08 sks cmt.
8/30/17 thru 8/31/17 thru 9/5/17 4.5" csg cut 5120' 5000' 4800' still not able to pull. 9/7/17 perforating two shots every 100' from 4800' to 3500'. Going to put cmt plug from 5120' to 3500'. 9/8/17 - Range had a spill. |
2635568 | Primary Facility | 2017-09-13 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | 8/28/17 Bottom plug set @ 7861' to 7328', 38.08 sks cmt.
8/30/17 thru 8/31/17 thru 9/5/17 4.5" csg cut 5120' 5000' 4800' still not able to pull. 9/7/17 perforating two shots every 100' from 4800' to 3500'. Going to put cmt plug from 5120' to 3500'. 9/8/17 - Range had a spill. 9/13/17 - perfed 2 shots every 100' 3500' to 2500'. TIH w/tubing and cmt. 3603' to 2500'. |
2636238 | Primary Facility | 2017-09-15 | Administrative/File Review | No Violations Noted | 8/28/17 Bottom plug set @ 7861' to 7328', 38.08 sks cmt.
8/30/17 thru 8/31/17 thru 9/5/17 4.5" csg cut 5120' 5000' 4800' still not able to pull. 9/7/17 perforating two shots every 100' from 4800' to 3500'. Going to put cmt plug from 5120' to 3500'. 9/8/17 - Range had a spill. 9/13/17 - perfed 2 shots every 100' 3500' to 2500'. TIH w/tubing and cmt. 3603' to 2500'. 9/15/17 - spoke w/Range rep. Aaron, they were able to circulate from their cut at 2500' and pull 4.5" csg. |
2636707 | Primary Facility | 2017-09-18 | Administrative/File Review | No Violations Noted | 8/28/17 Bottom plug set @ 7861' to 7328', 38.08 sks cmt.
8/30/17 thru 8/31/17 thru 9/5/17 4.5" csg cut 5120' 5000' 4800' still not able to pull. 9/7/17 perforating two shots every 100' from 4800' to 3500'. Going to put cmt plug from 5120' to 3500'. 9/8/17 - Range had a spill. 9/13/17 - perfed 2 shots every 100' 3500' to 2500'. TIH w/tubing and cmt. 3603' to 2500'. 9/15/17 - spoke w/Range rep. Aaron, they were able to circulate from their cut at 2500' and pull 4.5" csg. 9/18/17 - tagged cmt at 2510, 148 sks from 2504' to 1690'. 159 sks 1690' 845' and 167 sks 845' to surface. |
2640832 | Primary Facility | 2017-09-27 | Follow-up Inspection | In Compliance with Policy | Follow up inspection to a release incident that occurred on 9/7/2017. The Operator reported the release of 4 barrels of elevated water. Secondary containment was installed at the time of the incident. According to the Operators initial report, a small fraction of fluid was released to the ground. On 9/7/2017, The Operator collected water and soil samples of the fluid released and fluid from two small seeps, located on the right side of the well site. According to the Operator, the sample results do not indicate a that the fluid released was production fluid or contained any major constituent of concern other than Iron. The Operator contacted the Department on 9/26/2017 to schedule an inspection on 9/27/2017 to visually inspect the pad after the secondary containment was removed. At the time of inspection, the well was plugged. The Operator was working to remove the stone and secondary containment from the well site. During the inspection, the Department observed the secondary containment berm was installed |
2836266 | Primary Facility | 2019-02-05 | Site Restoration | No Violations Noted | Inspection conducted in response to a Post-Plugging Well Site Restoration Report received by Department.
A Landowner Consent form was also received with the restoration report submittal (photo #1). According to this form, the access road and well pad are to remain. At time of inspection well appears to be plugged. No erected monument present. According to Department records a buried plate is installed 36" below surface. Access road rocked. No E and S issues observed. Well pad rocked. No E and S issues observed. This restoration report is approved. |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
1447914 | 461610 | 05/09/2005 | 2005-05-09 | 201TAG - Failure to install, in a permanent manner, the permit number on a completed well | Administrative | |
1447914 | 461611 | 05/09/2005 | 2005-05-09 | 102.4 - Failure to minimize accelerated erosion, implement E&S plan, maintain E&S controls. Failure to stabilize site until total site restoration under OGA Sec 206(c)(d) | Environmental Health & Safety | |
1447914 | 461612 | 05/09/2005 | 2005-05-09 | 210UNPLUG - Failure to plug a well upon abandonment | Administrative | |
2113185 | 653006 | 10/18/2012 | 2012-10-18 | 212PRODRPT - Failure to submit production report | Administrative |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
461610 | 193464 | NOV - Notice of Violation | Comply/Closed | 2005-10-07 | |||
461611 | 193464 | NOV - Notice of Violation | Comply/Closed | 2005-10-07 | |||
461612 | 193464 | NOV - Notice of Violation | Comply/Closed | 2005-10-07 |
For data sources see[8]