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Well ID: 37-129-25283 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Westmoreland | |
Municipality: Washington Township | |
Operator Name: CNX GAS CO LLC | |
Well Pad ID: | |
Farm/Lease Name: P R U I TOWNSEND | |
License Status: Plugged and Abandoned | |
Spud Date: 2004-08-11 | |
Permit Date: 2004-06-08 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.547735 | |
Longitude: -79.614827 |
Date | Event |
---|---|
2004-06-08 | New Permit Application |
2004-08-09 | Performed Spud Operation |
2004-08-13 | Drilling Completion |
2004-10-07 | Perforation |
2005-09-13 | Newly Drilled |
2017-06-27 | Begin Plugging |
2017-07-03 | Finished Plugging |
2019-05-17 | Fully Plugged |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2005 | CONSOL GAS CO | 16142 | 365 | 0.00 | 0 | 0.00 | 0 |
2006 | CONSOL GAS CO | 6717.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2007 | CONSOL GAS CO | 5854.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2008 | CONSOL GAS CO | 3425.25 | 365 | 0.00 | 0 | 0.00 | 0 |
2009 | CONSOL GAS CO | 3952.79 | 365 | 0.00 | 0 | 0.00 | 0 |
2010 | CONSOL GAS CO | 2,174.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | CONSOL GAS CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | CNX GAS CO LLC | 1.00 | 366 | 0.00 | 0 | 0.00 | 0 |
2013 | CNX GAS CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2014 | CNX GAS CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2015 | CNX GAS CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2016 | CNX GAS CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2017 | CNX GAS CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2013 | CNX GAS CO LLC | Produced Fluid | 21.00 Bbl | INJECTION DISPOSAL WELL | 34-013-20609 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1367929 | Primary Facility | 2004-08-12 | Drilling/Alteration | No Violations Noted | Rig at 930ft. during inspection,pit ok,E&S ok |
1613082 | Primary Facility | 2007-04-02 | Routine/Complete Inspection | No Violations Noted | E&S OK. |
2605927 | Primary Facility | 2017-06-20 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Inspection performed in response to receipt of Notice of Intention to plug. At the time of inspection well plugging activity appears to have commenced. BMPs installed, no E&S issues. |
2623470 | Primary Facility | 2017-07-21 | Routine/Complete Inspection | No Violations Noted | At the time of inspection well plugging appears to have been completed and pending site restoration. E&S plan on site and no E&S issues. |
2717497 | Primary Facility | 2018-04-12 | Site Restoration | No Violations Noted | Inspection in response to receipt of well site restoration report. At the time of inspection well site appears to be restored. Vegetative cover on seeded area established. No E&S issues. |
For data sources see[7]