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Well ID: 37-131-20160 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Wyoming | |
Municipality: Nicholson Township | |
Operator Name: CHIEF OIL & GAS LLC | |
Well Pad ID: 149079 | |
Farm/Lease Name: POLOVITCH UNIT | |
License Status: Plugged and Abandoned | |
Spud Date: 2011-05-07 | |
Permit Date: 2011-05-03 | |
Well Type: GAS | |
Unconventional Well: Y | |
Configuration: Horizontal Well | |
Conservation: No | |
Latitude: 41.640767 | |
Longitude: -75.810972 |
Date | Event |
---|---|
2011-05-03 | New Permit Application |
2011-05-06 | Performed Spud Operation |
2011-06-12 | Drilling Completion |
2011-08-05 | Perforation |
2011-08-05 | Performed Stimulation |
2011-10-06 | DEVIATED |
2015-06-17 | Begin Plugging |
2018-11-08 | Finished Plugging |
2018-12-13 | Fully Plugged |
For data sources see[4]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 2011-08-23 | 2011-08-23 | 7,685 | 4,863,516 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | FRW-18 | BJ Services Company | Friction Reducer | |||||
Distillates, petroleum, hydrotreated light | 64742-47-8 | 10.05 | ||||||
Water | Base Fluid | Water | 100.00 | 74.93 | ||||
Scaletrol 720 | BJ Services Company | Scale Inhibitor | Diethylene glycol | 111-46-6 | ||||
Ethylene glycol | 107-21-1 | 0.04 | ||||||
Techni-Hib 604 | BJ Services Company | Oxygen Scavenger | Water | 7732-18-5 | 5.00 | |||
Ammonium bisulfite | 10192-30-0 | 75.00 | 0.01 | |||||
Alpha 1427 | BJ Services Company | Biocide | ||||||
Didecyl dimethyl ammonium chloride | 7173-51-5 | |||||||
Water | 7732-18-5 | |||||||
Ethanol | 64-17-5 | |||||||
Quaternary ammonium compounds, benzyl-C12-16-alkyldimethyl, chlorides |
68424-85-1 | |||||||
Glutaraldehyde | 111-30-8 | 0.02 | ||||||
Sand (Proppant) | BJ Services Company | Propping Agent | ||||||
Quartz | 14808-60-7 | 99.90 | 24.89 |
For data sources see[5]
Stimulation Date | Phase Number | Chemical Agent | Volume (gal) | Treating Pressure (psi) | Breakdown Pressure (psi) |
---|---|---|---|---|---|
2011-08-05 | 0 | 0 | 0 |
For data sources see[6]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2011 | CHIEF OIL & GAS LLC | 82,789.00 | 63 | 0.00 | 0 | 0.00 | 0 |
2012 | CHIEF OIL & GAS LLC | 273,749.77 | 362 | 0.00 | 0 | 0.00 | 0 |
2013 | CHIEF OIL & GAS LLC | 224,305.00 | 343 | 0.00 | 0 | 0.00 | 0 |
2014 | CHIEF OIL & GAS LLC | 113,302.00 | 248 | 0.00 | 0 | 0.00 | 0 |
2015 | CHIEF OIL & GAS LLC | 0.32 | 7 | 0.00 | 0 | 0.00 | 0 |
2016 | CHIEF OIL & GAS LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2017 | CHIEF OIL & GAS LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[7]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2011 | CHIEF OIL & GAS LLC | Fracing Fluid Waste | 12,620.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2011 | CHIEF OIL & GAS LLC | Drilling Fluid Waste | 615.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | EPA ID: 748-163 |
2011 | CHIEF OIL & GAS LLC | Drill Cuttings | 336.77 Tons | LANDFILL | 301626 |
2011 | CHIEF OIL & GAS LLC | Fracing Fluid Waste | 119.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0008451 |
2012 | CHIEF OIL & GAS LLC | Produced Fluid | 6,805.80 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2013 | CHIEF OIL & GAS LLC | Produced Fluid | 4,286.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2014 | CHIEF OIL & GAS LLC | Produced Fluid | 1,979.50 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2015 | CHIEF OIL & GAS LLC | Drilling Fluid Waste | 389.52 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NC018 |
2015 | CHIEF OIL & GAS LLC | Drilling Fluid Waste | 515.77 Bbl | LANDFILL | 301358 |
2016 | CHIEF OIL & GAS LLC | Fracturing Fluid Waste | 40.00 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123 |
2016 | CHIEF OIL & GAS LLC | Produced Fluid | 0.01 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2018 | CHIEF OIL & GAS LLC | Spent Lubricant Waste | 12.81 Bbl | LANDFILL | 301358 |
For data sources see[8]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1971802 | Primary Facility | 2011-05-09 | Drilling/Alteration | No Violations Noted | UDI Rig 58 Jim Quisenberry - co. man |
1973080 | Primary Facility | 2011-04-16 | Drilling/Alteration | No Violations Noted | drillers log checked, hit water @ 79', 1" stream @ 83' |
1976430 | Primary Facility | 2011-05-26 | Drilling/Alteration | No Violations Noted | UDI Rig 58 comp. man -Jim Quisenberry, tool/pusher- Bob |
1977709 | Primary Facility | 2011-06-03 | Drilling/Alteration | No Violations Noted | 9 5/8" @ 2991' w/ 630 sx , 15.6ppg 70 bbls returns to surf done 5/20/2011 |
1979331 | Primary Facility | 2011-06-07 | Drilling/Alteration | No Violations Noted | Fishing, dropped a jt. down hole |
1979364 | Primary Facility | 2011-06-03 | Routine/Complete Inspection | Violation(s) Noted | NERO EC&B technical review concurs with report conclusions that the impacted area was remediated to background concentrations for all parameters tested for without an MSC (strontium, chloride and calcium) and residential Statewide Health standard for barium, VOCs, and SVOCs. Act 2 release of liability cannot be granted for this incident since the report was submitted under the “alternative remediation” process, as described in the draft policy “Addressing Spills and Releases at Oil & Gas Well Site.” |
1980901 | Primary Facility | 2011-06-16 | Follow-up Inspection | Outstanding Violations - No Viols Req'd | |
1990417 | Primary Facility | 2011-07-25 | Routine/Complete Inspection | No Violations Noted | 2 vent pipes ( 5 1/2" X 8 5/8" annulus, & 8 5/8" X 13 7/8" annulus) running to frac tank. |
1998221 | Primary Facility | 2011-08-24 | Drilling/Alteration | No Violations Noted | Fracing, Comp. Man - Bill Burton |
1999478 | Primary Facility | 2011-08-30 | Drilling/Alteration | No Violations Noted | Fracing. Comp. Man - Bill Burton |
2005964 | Primary Facility | 2011-09-27 | Routine/Complete Inspection | No Violations Noted | |
2026243 | Primary Facility | 2011-12-09 | Complaint Inspection | No Violations Noted | In production, digital pressure guage = 1074 psi. |
2029346 | Primary Facility | 2011-12-15 | Complaint Inspection | Pending | On site w/ Eric Rooney to gather isotopic samples from annuli Chief Reps. on site are Rich Adams, Ralph Larson, and Jon Hafer. 2 annulus vents - cellar filled in w/ gravel. Will be dug up to identify annuli. |
2029351 | Primary Facility | 2011-12-19 | Follow-up Inspection | Violation(s) Noted | On site w/ Kewvin Costello. Met Chief Reps. Rich Adams, Jon Hafer. Cellar has been dug up to confirm which annuli the vents go to. |
2029352 | Primary Facility | 2011-12-22 | Follow-up Inspection | Outstanding Violations - No Viols Req'd | Met Ralph Larsen and Jon Hafer, Chief representatives. On site to take flow readings w/ oriface meter. Used the 1/4" plate. There are 2 vents on this well. Did not check the 9 5/8 X 5 1/2" annulus. The other vent goes to the 20 X 13 3/8 " and 13 3/8 X 9 5/8" both. Meter reading was 0" of water which = 0 cf/day gas. Also tried the 1/8" plate and got 0" of water, but could feel very small flow. |
2042690 | Primary Facility | 2011-06-29 | Administrative/File Review | No Violations Noted | Response to NOV and sampling data received. |
2051393 | Primary Facility | 2012-03-15 | Routine/Complete Inspection | Outstanding Violations - No Viols Req'd | 1200 psi on prod. |
2062417 | Primary Facility | 2012-04-12 | Routine/Complete Inspection | Outstanding Violations - No Viols Req'd | Producing well,1155 psi. |
2062428 | Primary Facility | 2012-03-27 | Routine/Complete Inspection | Outstanding Violations - No Viols Req'd | Producing. Cellar dug out, no water and 2 vents. |
2064978 | Primary Facility | 2012-04-27 | Routine/Complete Inspection | Outstanding Violations - No Viols Req'd | Prod - 1129 psi |
2067539 | Primary Facility | 2012-05-14 | Routine/Complete Inspection | Outstanding Violations - No Viols Req'd | Cellar partially dug out - no water. 2 annular vents - open. |
2077000 | Primary Facility | 2012-06-18 | Follow-up Inspection | Outstanding Violations - No Viols Req'd | Concrete barriers have been placed around well heads. |
2086701 | Primary Facility | 2012-07-24 | Follow-up Inspection | Outstanding Violations - No Viols Req'd | No change since last insp. about 3" water in cellar, no bubbles. 1150 psi on prod. 2 annular vents. Both open, vented. |
2087764 | Primary Facility | 2012-07-30 | Follow-up Inspection | Outstanding Violations - No Viols Req'd | This is a prod. well/ Has 2 annular vents, open. Clean water in cellar, no bubbles. |
2097239 | Primary Facility | 2012-08-30 | Follow-up Inspection | Outstanding Violations - No Viols Req'd | On site w/ Kevin Costello(DEP), Ralph Larson, (Chief) & Jon Hafer(Chief consult.) to witness flow tests and pressures on annuli. Shut in both annuli for 20 min. - 13 3/8 x 9 5/8" = 10 psi (Note: This vent may also contain the 20 x 13 3/8" annulus), and 9 5/8 x 5 1/2" has = 0 psi. Connected the orifice meter to the 13 3/8 x 9 5/8" annulus - readinf of 0 to 0.01 inches of water with 1/8" orifice plate which is equivalent to 5 cuft/day( barely detectable). |
2103131 | Primary Facility | 2012-09-14 | Follow-up Inspection | Outstanding Violations - No Viols Req'd | Producing well. Very little water in cellar. Cellar is dug out. 2 annular vents go to tank, both open and no pressure guages. 1150 psi on prod. Workers on site putting in larger pipeline and line to W. Polovitch. |
2155758 | Primary Facility | 2013-04-08 | Follow-up Inspection | Outstanding Violations - No Viols Req'd | Water in cellar. There are 2 annular vents on this well. Both are shut, in prep. for N/T logging on the 1 H. There is bubbling in the cellar. Bubbles appear to be coming from a connection on the vent of the 9 5/8 x 13 3/8" annulus. No presure guages are present on annular vents. |
2175542 | Primary Facility | 2013-06-11 | Routine/Complete Inspection | Outstanding Violations - No Viols Req'd | Producing well - 788 psi. 2 annular vents are open. |
2199493 | Primary Facility | 2013-08-14 | Routine/Complete Inspection | Outstanding Violations - No Viols Req'd | Producing well. |
2213510 | Primary Facility | 2013-10-01 | Follow-up Inspection | Outstanding Violations - No Viols Req'd | On site w/ Eric Rooney, DEP and Jon Hafer, Chief to collect isotopic samples from various annuli. Annuli were shut in yesterday at 4:30 PM so 17+ hours. |
2240212 | Primary Facility | 2014-01-24 | Routine/Complete Inspection | Outstanding Violations - No Viols Req'd | No activity on site. |
2321184 | Primary Facility | 2014-11-04 | Follow-up Inspection | Violation(s) Noted | |
2670027 | Primary Facility | 2017-12-11 | Routine/Complete Inspection | No Violations Noted | There was no activity occurring at the site at the time of the inspection. I was accompanied by Jon Sassi (EPS) and consulted with Ken Kennedy (OGI). No violations were noted pertaining to this well. If you have any questions, please contact me. |
2703210 | Primary Facility | 2018-02-22 | Compliance Evaluation | In Compliance with Schedule | Arrived onsite at 15:15. Onsite to check on progress of re plumbing of all (4) wells annular vents to surface in preparation for long term venting phase as discussed and agreed to in the Depts. meeting with Chief O&G of 2/14/18. All (4) wells, the Polovitch 1H, 1V, 4H and 5H, have had their (20" x 13 3/8"), (13 3/8" x 9 5/8") and (9 5/8" / WB) annular vents plumbed to surface via 2" vents. Vents had been fitted with ball valves and Tees w/ needle valves to access vents for sampling and eventual PBUTs. The Dept. will be meeting Chief O&G Rep., Jon Hafer back at pad tomorrow morning at 09:30 to obtain gas samples off all annuli, where gas is present, for Isotopic analysis. Chief O&G has had all annular spaces and vents purged of fluid and were shut in earlier today in preparation for tomorrows sampling event. (See attached, "As Plugged" Well Bore Schematics for individual wells for plugging details as of 2/14/18).
All previous, deteriorated pad liner and debris have been removed from location. Location was fo |
2703221 | Primary Facility | 2018-02-23 | Compliance Evaluation | In Compliance with Schedule | Arrived onsite at 09:00. Upon arrival met up with Chief O&G Rep., Jonathan Hafer and D.E.P. Geologist, Eric Rooney. Onsite to initiate the 1st long term, approx. 90 day, venting period as agreed to in meeting of 2/14/18 with Chief O&G. All (4) wells annuli vents, the (20" x 13 3/8"), (13 3/8" x 9 5/8") and (9 5/8" / WB) were re-plumbed to surface and shut-in yesterday in preparation for todays sampling. Mr. Hafer explained that he would be taking gas samples off all the wells annular vents to send off for analysis. Following Mr. Hafers collection of annuli samples, I performed gas screenings at all (4) wells annuli using a ALTAIR 5X gas meter calibrated on 2/5/18. Gas was detected at the following wells annuli:
1H: (13 x 9) = 100% LEL, 100% CH4, 4H: (13 x 9) = 100 % LEL, 30 % CH4, 5H: (13 x 9) = 100 % LEL, 8 % CH4, Following sample collection and gas screenings, all (4) wells annuli were opened to vent to atmosphere. This long term venting period will extend for ~ 90 days. Operator will then be performing |
2775961 | Primary Facility | 2018-08-31 | Compliance Evaluation | In Compliance with Schedule | Arrived onsite at 11:00. Upon arrival met with Chief O&G Rep., Jonathan Hafer to conclude the 7 day PBUTs being performed on all (4) wells annuli vents, the (20" x 13 3/8"), (13 3/8" x 9 5/8") and (9 5/8" / WB). This is the 2nd PBUT being performed after (2) full 90 day, long term venting periods. Pre-shut in test gas screenings were performed at all wells annular vents on 8/24/18 by Mr. Hafer using a Rae Systems Multi-Rae gas meter, calibrated that morning. The only annuli where gas was detected are listed below:
1H: (13x9) = 3.1% CH4, 51% LEL 1V: (9/WB) = 1.6% CH4, 36% LEL 4H: (13x9) = 1.9% CH4, 70% LEL 5H: (13x9) = 6.6% CH4, 100% LEL Today, the ending 7 day PBUT results were: 1H: (20x13)= 0.40 psi, (13x9)= 12.95 psi, (9/WB)= 0.44 psi. 1V: (20x13)= -0.10 psi, (13x9)= -2.0 psi, (9/WB)= 0.45 psi. 4H: (20x13)= 0.10 psi, (13x9)= 11.10 psi, (9/WB)= 0.70 psi. 5H: (20x13)= 0.65 psi, (13x9)= 5.2 psi, (9/WB)= 0.75psi. - Mr. Hafer explained that he would be collecting samples off all the wells annular vents to sen |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
1979364 | 613129 | 06/03/2011 | 2011-06-03 | 402CSL - Failure to adopt pollution prevention measures required or prescribed by DEP by handling materials that create a danger of pollution. | Environmental Health & Safety | Referred to ECP |
1979364 | 613130 | 06/03/2011 | 2011-06-03 | 78.56(1) - Pit and tanks not constructed with sufficient capacity to contain pollutional substances. | Administrative | |
1979364 | 614844 | 06/03/2011 | 2011-06-03 | 601.101 - O&G Act 223-General. Used only when a specific O&G Act code cannot be used | Administrative | SWMA 6018.301, 210 - 252 gallons drilling mud spilled on ground surface, connection on a Kelly Hose failed. |
2029351 | 627798 | 12/19/2011 | 2011-12-19 | 78.86* - Failure to report defective, insufficient, or improperly cemented casing w/in 24 hrs or submit plan to correct w/in 30 days | Administrative | GMI COA executed 10/23/2017. |
2321184 | 710148 | 11/04/2014 | 2014-11-04 | 78.73A - Operator shall prevent gas and other fluids from lower formations from entering fresh groundwater. | Environmental Health & Safety | Actually 78.73(b) |
2321184 | 710149 | 11/04/2014 | 2014-11-04 | 78.81D1 - Failure to maintain control of anticipated gas storage reservoir pressures while drilling through reservoir or protective area | Administrative | Actually 78.81(a)(2)+(3) |
2321184 | 710150 | 11/04/2014 | 2014-11-04 | 78.85 - Inadequate, insufficient, and/or improperly installed cement | Environmental Health & Safety | Actually 78.85(a)(5) |
2321184 | 710151 | 11/04/2014 | 2014-11-04 | 78.86* - Failure to report defective, insufficient, or improperly cemented casing w/in 24 hrs or submit plan to correct w/in 30 days | Administrative | |
2321184 | 799776 | 11/04/2014 | 2014-11-04 | CSL 401 - PROHIBITION AGAINST OTHER POLLUTIONS - Discharged substance of any kind or character resulting in pollution of Waters of the Commonwealth. | Environmental Health & Safety |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
613129 | 272349 | NOV - Notice of Violation | Comply/Closed | 2013-11-21 | |||
613130 | 272349 | NOV - Notice of Violation | Comply/Closed | 2013-11-21 | |||
614844 | 272349 | NOV - Notice of Violation | Comply/Closed | 2013-11-21 | |||
627798 | 279011 | NOV - Notice of Violation | |||||
710148 | 317500 | NOV - Notice of Violation | |||||
710148 | 358810 | COA - Consent Order and Agreement | 2017-10-23 | $178,622.00 | $178,622.00 | ||
710149 | 317500 | NOV - Notice of Violation | |||||
710149 | 358810 | COA - Consent Order and Agreement | 2017-10-23 | $178,622.00 | $178,622.00 | ||
710150 | 317500 | NOV - Notice of Violation | |||||
710151 | 317500 | NOV - Notice of Violation | |||||
710151 | 358810 | COA - Consent Order and Agreement | 2017-10-23 | $178,622.00 | $178,622.00 | ||
799776 | 317500 | NOV - Notice of Violation | Administrative Close Out | 2017-10-23 | |||
799776 | 358810 | COA - Consent Order and Agreement | 2017-10-23 | $178,622.00 | $178,622.00 |
For data sources see[9]